Bakersfield Municipal Airport, California
Location: The Bakesfield Municipal Airport is
located 3 miles south of Bakersfield, California.
History: Bakersfield Municipal Airport,
known at the time as Oildale Field, or Bakersfield
Army Air Field, was home to combat ready Army Air
Forces fighter units tasked with defense of
California in 1941.
After the first threat of enemy attack during World War II had subsided,
the field was used as a sub base for Hammer Field in Fresno by the 4th Air
Force for pilot training.
In 1945, new Jet powered YP-80As were delivered to the 412th Fighter
Group for service tests. The group was relocated to Santa Maria Air
Field in 1945.
Bakersfield Municipal Airport Today: Intensive
flight training; Helicopter and military operations;
Airport
Services and Amenities: Fuel; Air BP 100LL; Self service 24 hours; Kern
Charter Service;
Special Events and
Attractions: Museum; Arena; Kern County Fairgrounds; Mesa Marin Raceway;
Airport
Area Accident History:
Accident occurred Sunday, September 30, 2007 in
Bakersfield, CA
Probable Cause Approval Date: 10/31/2007
Aircraft: Cessna 182F, registration: N3580Y
Injuries: 4 Uninjured.
The airplane porpoised on the runway while
decelerating during a rejected takeoff. The pilot did not have the Cessna
issued gust lock that fits into the hole in the control yoke. Therefore, he
placed a machine bolt into the hole to keep the flight controls steady while
he washed his airplane. During the pilot's subsequent preflight and
pre-takeoff check he failed to observe that movement of the flight controls
was restricted. During takeoff, as the airplane became airborne, the bolt's
presence was discovered, and the pilot retarded the throttle. The airplane
contacted the runway in a nose low attitude and porpoised, thereby bending
the firewall and fuselage.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's inadequate preflight inspection and
pre-takeoff checks during which he failed to remove the gust lock.
===
Accident occurred Wednesday, August 29, 2007 in
Bakersfield, CA
Probable Cause Approval Date: 12/20/2007
Aircraft: Cessna 172S, registration: N3544Z
Injuries: 1 Uninjured.
In a telephone interview with the NTSB
investigator-in-charge approximately 45 minutes after the accident, the
student pilot reported that after landing on Runway 30R the airplane started
to veer to the left. The student pilot stated that he was trying to correct
back to the right "...but the right wing went up and the airplane went off
the left side of the runway." The student pilot reported that the right main
landing gear failed and the airplane came to rest in an upright position
about 30 feet off the runway. The student pilot stated that there was damage
to the right wing tip, the right horizontal stabilizer and the right
elevator. The student pilot said, "I just lost control of the airplane." In
an interview with the IIC, the airport manager revealed that the airplane
had impacted a taxiway sign. At 0854, the on airport automated weather
facility reported wind from 170 degrees at 4 knots, visibility 10 statute
miles, sky clear, temperature 30
degrees C, dew point 12 degrees C, and an altimeter
setting of 29.87 inches of Mercury.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The student pilot's failure to maintain directional
control of the airplane during the landing roll, which resulted in a
collision with a taxiway sign.
===
Accident occurred Tuesday, June 05, 2007 in
Bakersfield, CA
Probable Cause Approval Date: 8/30/2007
Aircraft: Cessna T210N, registration: N6973N
Injuries: 2 Uninjured.
The pilot reported that as he was turning on to base
leg for Runway 30R he noticed that the wind was stronger than anticipated,
and when established on final the wind had caused the airplane to drift to
the right of the runway's centerline. The pilot stated that as he was making
adjustments to line up with the centerline the air traffic controller
instructed him to go around. As he was pitching up and adding power the
controller then told the pilot he was cleared to land, prompting the pilot
to reduce power, drop the nose, and continue to make adjustments for the
crosswind. The pilot reported that when the airplane touched down it bounced
two or three times, "...then a strong wind gust caused the plane to exit the
runway to the right." As a result of the nose wheel collapsing aft the
firewall sustained substantial damage. The pilot estimated winds from 270
degrees between 12 and 14 knots, with wind gusts to 18 knots.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's improper flare, which resulted in a loss
of directional control. Factors included the crosswind and gusty wind
condition.
===
Accident occurred Saturday, December 09, 2006 in
Bakersfield, CA
Probable Cause Approval Date: 5/28/2008
Aircraft: John Lauer Harmon Rocket II, registration:
N604JL
Injuries: 2 Fatal.
Witnesses reported seeing the airplane performing
aerobatic maneuvers just prior to the accident. As the airplane was
completing a loop, it impacted terrain in a wings level, nose high attitude.
There was no evidence of pre-impact mechanical malfunctions observed during
the subsequent examination of the engine or the control system that would
have precluded normal operation.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's failure to maintain terrain clearance
during an aerobatic maneuver.
===
Accident occurred Tuesday, July 18, 2006 in
Bakersfield, CA
Probable Cause Approval Date: 10/31/2006
Aircraft: Beech A36, registration: N4785M
Injuries: 3 Uninjured.
The pilot made a hard landing resulting in
substantial damage to the airplane. The pilot extended his downwind for
landing at the destination airport with the intention of avoiding the wake
turbulence produced by a jet departing the runway of intended use. While in
the landing flare, the pilot stalled the airplane, resulting in a hard
landing. The right main landing gear collapsed and the airplane rolled off
the runway surface. The pilot reported no pre-impact mechanical malfunctions
or failures with the airplane that would have precluded normal operation.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's improper flare, which resulted in a hard
landing.
===
Accident occurred Thursday, November 17, 2005 in
Bakersfield, CA
Probable Cause Approval Date: 3/28/2006
Aircraft: Piper PA-28RT-201, registration: N2863X
Injuries: 1 Uninjured.
The airplane landed hard on the displaced threshold
of the runway while maneuvering on short final approach to properly align
with the runway. The pilot reported that she had to make a slight s-turn to
final approach to correct for overshooting the runway centerline. As she
flared, the airplane would not respond to control input and impacted the
displaced threshold hard and skidded to rest on the right side of and short
of the runway. Air traffic controllers asked the pilot to make a short final
for traffic considerations and she accepted the request. They observed the
airplane overshoot the runway centerline and enter a steep bank in an effort
to realign with final approach. The airplane descended rapidly and impacted
the ground. Post-accident examination of the airplane by a Federal Aviation
Administration airworthiness inspector, and a local mechanic, revealed no
pre-impact anomalies with the airplane that would have prevented its normal
operation. The
airplane sustained structural damage to both wings
and the fuselage. The landing gear were sheared from the airplane.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's failure to maintain adequate airspeed,
which resulted in an accelerated stall and hard landing.
===
Accident occurred Wednesday, May 25, 2005 in
Bakersfield, CA
Probable Cause Approval Date: 8/29/2006
Aircraft: Bell 47G-4A, registration: N110DT
Injuries: 1 Serious.
The helicopter collided with power lines and crashed
in a cotton field while conducting aerial application operations. The pilot
completed his first pass from west to east across the north end of the
potato field. As he came in for his second pass, the helicopter struck power
lines that ran north and south along the west side of the potato field. The
helicopter came down in an adjacent cotton field. The pilot said he saw the
power lines just prior to striking them.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's inadequate visual lookout and failure to
maintain clearance from the power lines.
===
Accident occurred Wednesday, April 20, 2005 in
Bakersfield, CA
Probable Cause Approval Date: 4/25/2006
Aircraft: Bailey Lowing Loadster, registration:
N8058Q
Injuries: 1 Serious.
The experimental airplane impacted a fence and a
storage facility following a loss of engine power while on the downwind leg
of the traffic pattern. The private pilot, who was the builder of the
airplane, indicated he used a Volkswagen engine that he overhauled to power
his airplane. According to the pilot, he wanted to break in the overhauled
engine with 25 hours of operation in flight, but since the airplane was just
built, he had to conduct a lot of high-speed taxi tests and takeoff and
landings. Therefore, the pilot believed the engine did not receive an
adequate break in. While on the airplane's fourth test flight, the pilot
experienced a gradual loss of power while on downwind for the second
approach. Post accident examination of the aircraft/engine by the pilot
revealed scoring on the pistons, which was the only anomaly noted. The pilot
was unable to test the carburetor due to damage sustained in the accident.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the loss of engine power for undetermined reasons.
===
Accident occurred Monday, May 03, 2004 in
Bakersfield, CA
Probable Cause Approval Date: 6/28/2006
Aircraft: Bell OH-58A+, registration: N397E
Injuries: 2 Uninjured.
The helicopter collided with power lines and landed
hard during a night autorotation following a loss of engine power. As the
pilot initiated a turn, both he and the observer heard a loud boom. While
they were discussing the origin of the boom, a second boom occurred followed
by an immediate power loss. The pilot lowered the collective and entered an
autorotation. During the flare, he realized he was going to overshoot the
landing zone (LZ) and lined up with a street for landing. The pilot
initiated a flare about 60 feet above the ground and felt a strong jolt with
an increased rate of descent and a loss of main rotor rpm's as the
helicopter collided with power lines. The helicopter landed hard from about
10 feet above the ground. Review of the maintenance logbooks revealed that
the engine had been in service 5 months and 161 hours since a 1,750-hour
inspection had been completed. An engine teardown was conducted. Various
internal components had
excessive heat damage, carbon deposits, and metal
splatter. There was a partial loss of airfoils for the number 1 turbine
wheel. The gas producer (GP) turbine could not be manually rotated and was
locked in place, with the second-stage turbine nozzle diaphragm fractured
into several pieces. Paperwork obtained from the engine overhaul facility
indicated that the second-stage turbine nozzle diaphragm had been replaced
by machining out the old diaphragm and brazing in a new diaphragm. A
metallurgical examination of the diaphragm revealed that it had separated
from the main portion of the nozzle at the braze joints and it was also
fractured 360 degrees around the trailing edge side of the diaphragm. The
fracture surface revealed no pre-existing cracks, and the damage was
determined to be consistent with tensile overstress. Both the leading and
trailing edges of the braze alloy fill were measured. The leading edge side
had a fill between 10 and 50 percent of
the joint width with an estimated average fill of 30
percent. The trailing edge side had a fill between 50 and 100 percent of the
joint width with an estimated average fill of 75 percent. The diaphragm's
manufacturer indicated that the braze alloy fill should fill the exposed
extremities in a continuous line for the first 20 percent of the joint
width, or 1.5 times the thickness of the thinnest member being joined, and
have a minimum total coverage of 80 percent of the joint. The braze
thickness of the accident diaphragm was measured to be at least 0.009-inch
in one location. The manufacturer's specifications for the braze thickness
was between 0.002 and 0.004-inches. Review of the overhaul facilities
procedures for the repair of the diaphragm included requirements for visual
and fluorescent penetrant inspection of the brazed joints after repair
completion. The Safety Board metallurgist found that those methods of
inspections were not capable of
detecting internal voids, unless the voids were
connected to the surface. The manufacturer and the overhaul facility
reviewed the history and processing of the diaphragm. It was noted that
normally the overhaul facility used the hydrogen fluoride cleaning method to
clean the majority of the diaphragms prior to brazing. However, the accident
diaphragm and seven others were cleaned using the vapor degreasing method.
Other diaphragms that had undergone the vapor degreasing method were
retrieved and destructively examined. The results showed that these
diaphragms contained cracking along the brazed joints. Several diaphragms
that had undergone the hydrogen fluoride cleaning method were retrieved and
destructively examined. They contained no cracks; however, the braze
thickness was noted to be as large as 0.020 inches. As a result of the
accident, the manufacturer revised their Parts Repair Procedures Letter
(PRPL 2-D004) to reflect changes in the procedures
for brazing the second-stage turbine nozzle
diaphragm, which included hydrogen fluoride cleaning, and immersion
ultrasonic inspection and ultrasonic inspection during and after the brazing
process. The overhaul facility rewrote their procedures to reflect the
manufacturer's revised procedures.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
loss of engine power due to the separation of the
diaphragm portion of the repaired second-stage turbine nozzle from the rim
portion due to the use of an inadequate cleaning method to clean the joint
prior to the braze repair during overhaul by the manufacturer's authorized
maintenance center. Contributing to the accident was the lack of an
inspection procedure that could verify that the joint met the braze fill
requirements.
===
Accident occurred Saturday, April 03, 2004 in
Bakersfield, CA
Probable Cause Approval Date: 12/28/2004
Aircraft: Bell 47G-4A, registration: N7NB
Injuries: 1 Serious.
The helicopter experienced a loss of tail rotor
control and collided with terrain. During an aerial application flight, the
pilot heard a rattling noise from the aft end of the helicopter. He then
lost tail rotor authority and entered a flat spin. The pilot attempted to
make a run-on landing, but the helicopter continued to spin until it
impacted terrain. A Federal Aviation Administration inspector examined the
helicopter after the accident. He noted that the cross-over support tube
near the aft end of the tail boom was missing. A crack was found on the tail
boom left side frame tubes. Deposits of rust in the area suggests that the
crack was a pre-existing crack. The inspector thought that this would have
added excessive stress to the structure during turning maneuvers and caused
the last spline coupling shaft to disconnect from the tail rotor gear box as
the tail boom flexed. A 50-hour maintenance inspection was completed the day
before the accident.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
a loss of tail rotor drive due to a disconnection of
the drive shaft's splined coupling at the tail rotor gear box. The splined
coupling to tail rotor gear box disconnection occurred as a result of tail
boom flexing due to the combined effects of an uninstalled structural
support tube and a crack in left side frame tubes. Inadequate maintenance
inspection was a factor.
===
Accident occurred Sunday, August 25, 2002 in
Bakersfield, CA
Probable Cause Approval Date: 6/8/2005
Aircraft: Hispano Aviacion HA-200 SAETA,
registration: N232DS
Injuries: 2 Uninjured.
The ex-military jet trainer experienced a dual
engine flame out during cruise flight and it collided with multiple
obstacles during an attempted forced landing to a closed airport. The
airplane had not flown for 5 years until a new owner bought it. After an
annual inspection, the airplane was to be flown from Lewiston, Idaho, to Los
Angeles, California, in two legs. The first leg from Lewiston to Minden,
Nevada, used 352 gallons of fuel (full fuel is 367 gallons) and when the
airplane arrived, the hydraulic gear extension system malfunctioned and the
gear was extended using the emergency blow down system. The pilot then
decided to continue on the second leg with the gear locked in the down
position. Ninety minutes into the second leg the pilot became concerned
about the amount of fuel remaining and was diverting to Bakersfield when
both engines flamed out. The pilot was attempting a dead stick landing at a
closed airport when the right wing struck the
ground and then the left wing struck a telephone
pole. First responders noted about 80 gallons of fuel had spilled on the
ground from the separated left tip tank. No fuel was found in the right tip
tank or either of the fuselage tanks. The fuel system consists of two tip
tanks; one aft fuselage tank, and a forward fuselage tank. The tip tanks,
which feed only into the aft fuselage tank, are used by porting engine bleed
air to the tanks through a pneumatic switch in the cockpit. The switch has
positions for LEFT, RIGHT, BOTH and OFF. The forward and aft fuselage tanks
are fed to the engines by conventional boost pumps. The proper fuel tank
usage sequence is to select the aft fuselage tank while selecting and
pressurizing both tip tanks, which then replenish the aft fuselage tank.
When the fuel from the both tip tanks and the aft fuselage tank is used,
then the forward fuselage tank is selected. Without at least one engine
operating, bleed air is not
available to pressurize the tip tanks to use any
fuel remaining there. No discrepancies were found during an examination of
the airframe, engines, or the fuel system components, including the tip tank
pressurization system, the boost pumps, or selector valves/switches. The
passenger, who holds pilot and A & P certificates stated that the pilot was
individually selecting the tip tanks (left or right) during flight and did
not use the BOTH position.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's improper fuel system management, which
lead to fuel starvation, and a loss of engine power. A factor in the
accident was the pilot's decision to continue on the second leg of the
flight with the gear in the extended position, which increased the fuel
consumption and reduced the aircraft's available range.
===
Incident occurred Wednesday, June 27, 2001 in
Bakersfield, CA
Probable Cause Approval Date: 2/25/2003
Aircraft: Beech A36, registration: N808NH
Injuries: 4 Uninjured.
During the landing approach on an instructional
flight, the certified flight instructor (CFI) initiated a go-around and
experienced restricted elevator control movement. The elevator control
became partially jammed in a nose low and then a nose high position. Roll
and yaw control was not affected. Using considerable force, the CFI
maintained airplane control and landed without additional incident.
Thereafter, the airplane was inspected. Evidence of mechanical binding to
the elevator pitch control cables was noted. Specifically, a screwdriver was
found wedged between the nose gear actuator retract rod and the elevator
control cables beneath the forward spar cover, between and under the pilots'
seats. When the nose gear retracted, the nose gear actuator retract rod
moved the screwdriver against the elevator control cable resulting in
binding. Upon removal of the screwdriver, the elevator operation was normal.
Two days prior to the incident, a contract
mechanic had performed maintenance on the airplane.
The maintenance required taking off the forward spar cover to allow removal
and installation of a flap motor gearbox assembly and flap flex drives.
Since this maintenance, the airplane had been operated 5.8 flight hours.
The National Transportation Safety Board determines
the probable cause(s) of this incident as follows:
During landing approach, mechanical binding of the
elevator control cable occurred due to a contract mechanic's improper
maintenance.
===
Accident occurred Saturday, December 23, 2000 in
BAKERSFIELD, CA
Probable Cause Approval Date: 11/6/2001
Aircraft: Cessna 140, registration: N72970
Injuries: 2 Minor.
During a forced landing precipitated by fuel
starvation and a loss of engine power, the airplane collided with a fence
and overturned. The engine stopped producing power about 2 miles from the
airport, and the pilot thought he could make it to the airport. About 500
feet above the ground, he noticed the airport boundary fence. He felt he
might strike it with the landing gear while in flight, so he decided to land
short of the airport. After the airplane came to rest, the pilot saw fuel
leaking from the inverted wing fuel tanks and evacuated the airplane. The
pilot did not recall moving the fuel selector valve after landing. The fuel
selector valve pointed to a position 20 to 30 degrees left of the right fuel
tank position. It pointed to the middle of a placard that indicated right
tank. However, a mechanic said he felt this position would not allow either
tank to supply sufficient fuel to the engine. He observed a flexible detent
that was installed to
ensure proper position of the fuel selector valve
when the right fuel tank was selected. The flexible detent bent down and was
not useable.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's inadequate in-flight planning, fuel
management, and inadequate remedial actions, which resulted in a total loss
of engine power due to fuel starvation. The pilot made an off-field landing
and collided with a fence.
===
Accident occurred Friday, August 11, 2000 in
BAKERSFIELD, CA
Probable Cause Approval Date: 11/1/2001
Aircraft: Barclay/Vincent MURPHY SR 2500,
registration: N24VW
Injuries: 2 Fatal, 2 Serious.
During an emergency landing the left wing of the
airplane struck an irrigation standpipe, and the airplane was destroyed in a
post impact fire. The pilot reduced the power to descend and circle to land
at a dirt airstrip. When he advanced the throttle to arrest the airplane's
descent there was no corresponding power increase. He conducted the
emergency procedures, but was unable to restart the engine. He overflew the
airstrip and attempted an emergency landing in a cornfield. Review of the
airplane's power plant logbook revealed that an overhauled engine had been
installed on the experimental airplane in March 1999. The last entry was
December 8, 1999, when the engine was test ran, and the fuel injection
system was adjusted according to manufacturer's specifications. No further
entries were found in the airframe or power plant logbooks. During the
engine examination the throttle valve was found jammed in the closed
position. Investigators also found the
idle speed stop screw backed off from the throttle
shaft arm about 1/8 inch. No further mechanical anomalies were noted.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
Adjustment by other maintenance personnel of the
idle speed stop screw. The idle speed stop screw was backed off from the
throttle shaft arm, not allowing the butterfly valve to operate properly,
which resulted in the butterfly valve remaining closed during a power input
via the throttle control linkage during the approach to landing phase.
Bakersfield Municipal
Airport Approach / Landing: