Camarillo Airpark, Camarillo, California
Location:
Camarillo Airpark is located 3 miles west of
Camarillo, California.
History:
Camarillo Airpark
Today: Obstructions reported; Unlighted Mountains;
Airport
Services and Amenities: Channel Islands Aviation; SkyBlueAir, Inc.;
Sun Air Jets; Western Cardinal, Inc.
Restaurant on the field; Waypoint Cafe; Lodging within 1 mile;
Special Events and
Attractions: Factory Outlet Stores; Commemorative Air Museum on
the field;
Airport
Area Accident History:
Accident occurred Tuesday, September 02,
2008 in Camarillo, CA
Aircraft: Lancair Propjet, registration:
N750PJ
Injuries: 2 Minor.
This is preliminary information, subject to
change, and may contain errors. Any errors in this report will be corrected when
the final report has been completed.
On September 2, 2008, about 1645 Pacific
daylight time, a Lancair Propjet single-engine amateur built airplane, N750PJ,
was substantially damaged during a forced landing following a loss of engine
power during the initial climb after takeoff from the Camarillo Airport (CMA),
Camarillo, California. The commercial pilot and his passenger sustained minor
injuries. The airplane was registered to Sierra Pacific Holdings Inc. of Malibu,
California and operated by the pilot under the provisions of Title 14 Code of
Federal Regulations (CFR) part 91. Visual meteorological conditions prevailed
and no flight plan was filed for the personal flight. The local flight was
originating at the time of the accident.
The pilot reported that during the initial
climb from runway 26, as the airplane passed about midfield at an altitude of
about 1,000 feet above ground level, the engine lost power. The pilot initiated
a forced landing and performed a 180-degree turn back to the runway. The pilot
landed within the runway overrun area beyond the departure end of the runway.
During the landing roll, the airplane struck a dirt pile and nosed over.
Examination of the airplane by an Federal
Aviation Administration inspector revealed that the outboard three feet of the
left wing was mostly separated and the rudder was partially separated from the
vertical stabilizer. Fuel was observed leaking from the airplane at the accident
site.
= = =
Accident occurred Sunday, August 31, 2008 in
Camarillo, CA
Aircraft: Piper PA-18-150, registration:
N7482D
Injuries: 1 Fatal.
This is preliminary information, subject to
change, and may contain errors. Any errors in this report will be corrected when
the final report has been completed.
On August 31, 2008, about 0926 Pacific
daylight time, a Piper PA-18-150, N7482D, sustained substantial damage after
impacting terrain while maneuvering at the Camarillo Airport (CMA), Camarillo,
California. The commercial pilot, the airplane's sole occupant, was killed. The
airplane was operated by Van Wagner Aerial Media of Hollywood, Florida, in
accordance with 14 Code of Federal Regulations Part 91. Visual meteorological
conditions prevailed for the local banner tow flight, and a flight plan was not
filed. The flight departed CMA about 5 minutes prior to the accident.
According to witnesses who observed the
accident, the airplane approached the banner tow pickup area at an elevation of
about 20 to 30 feet above ground level. One witness reported that after hooking
the banner the airplane pitched up to a 45-degree angle before leveling off at
about 200 feet above the ground. The witness stated that the airplane flew
straight and level for about 4 to 5 seconds, then suddenly nosed over to about a
30-degree angle before descending and impacting terrain. Another witness, a
certified flight instructor, reported that the airplane did not appear to stall,
and there was nothing to indicate that the airplane had entered a spin prior to
impacting terrain. There was no postcrash fire.
The wreckage was recovered for further
examination.
= = =
Accident occurred Thursday, July 10, 2008 in
Camarillo, CA
Probable Cause Approval Date: 8/28/2008
Aircraft: Piper PA-18A-150, registration:
N7471D
Injuries: 1 Uninjured.
The pilot stated that he was descending on a
5-mile final approach for the runway when the airplane experienced a total loss
of engine power. He said that there were no abnormal indications on the engine
gauges, and he believed he had exhausted all useable fuel in the two right wing
fuel tanks. He immediately switched the fuel selector to the left wing tank. The
engine did not regain power, so the pilot verified that the magneto switches
were on. According to the pilot, there is no electric starter installed on the
engine. The airplane continued to descend, and about 500 feet above the ground,
the propeller stopped rotating. The pilot released the banner he was towing, and
he made a forced landing in a rough field. The airplane nosed over during the
landing rollout, and the left wing's structure was damaged. The pilot reported
that the airplane was equipped with three fuel tanks, two in the right wing and
one in the left wing. Each tank holds 18 gallons
of fuel, for a total of 54 gallons that
provides about a 6-hour endurance. During banner tow operations the fuel burn
off rate is about 8 gallons per hour. All fuel tanks were filled to capacity
prior to the pilot's 1040 takeoff. The airplane had been airborne about 4 hours
when the loss of power occurred.
The National Transportation Safety Board
determines the probable cause(s) of this accident as follows:
The pilot's inadequate fuel management,
which resulted in a total loss of engine power due to fuel starvation.
= = =
Accident occurred Friday, October 26, 2007
in Camarillo, CA
Probable Cause Approval Date: 12/20/2007
Aircraft: Beech A36, registration: N16SF
Injuries: 2 Uninjured.
The airplane impacted the ground during an
attempted go-around. The pilot flew the approach at a higher altitude than
anticipated but decided to continue. Prior to landing, about 30 feet agl, the
local air traffic controller instructed the pilot to perform a go-around. The
pilot initiated the procedure with application of full throttle, and he
increased the airplane's pitch attitude. When the pilot saw he was gaining
altitude, he retracted the landing gear and the flaps. The airplane then stalled
and impacted the runway.
The National Transportation Safety Board
determines the probable cause(s) of this accident as follows:
The pilot's failure to maintain an adequate
airspeed during a go-around, which resulted in a stall.
= = =
Accident occurred Sunday, July 15, 2007 in
Camarillo, CA
Probable Cause Approval Date: 5/28/2008
Aircraft: North American F-51D,
registration: N51TK
Injuries: 1 Fatal.
The pilot was making his first supervised
solo flight in the same airplane that he received 31.5 hours of dual instruction
in the 47 days preceding the accident. The flight instructor who provided the
training witnessed the accident and reported that the pilot performed a "normal"
takeoff followed by a left pattern to runway 26 with a "normal tail low wheel
landing." He noted that as the airplane made contact with the ground, the pilot
"had not pulled his throttle back to idle, as the noise level of the engine
appeared greater than idle." After rolling 50 to 100 feet, the tail appeared to
rise slightly, indicating the pilot was applying slight forward stick to pin the
airplane to the ground. This was followed quickly by the rapid lowering of the
tail to the point where the tailwheel struck the ground with a "loud bang
noise." The airplane then "leaped back into the air" and the pilot applied
takeoff power. The airplane pitched nose high and rolled left to the inverted
position consistent with a torque induced roll. The upper surface of the left
wing contacted the ground first, followed by the propeller and the canopy. The
instructor expressed the opinion that the pilot "failed to successfully execute
a standard go-around procedure after experiencing unexpected flight due to the
lowering of the tail prematurely with power still on after touchdown."
The National Transportation Safety Board
determines the probable cause(s) of this accident as follows:
The pilot's failure to maintain aircraft
control during a go-around. Contributing to the accident was the pilot's lack of
experience in the make and model of airplane.
= = =
Accident occurred Sunday, March 25, 2007 in
Camarillo, CA
Probable Cause Approval Date: 5/29/2007
Aircraft: Boykin Rotorway Exec 162F,
registration: N496SB
Injuries: 1 Uninjured.
The pilot said that this was his first solo
flight in this make and model helicopter. He said he did weight and balance
calculations before performing a preflight inspection of the aircraft. The pilot
said that he performed a ground taxi, and hovered for 5 to 10 minutes, with
pedal turns, to check the control capability. He flew to an open field and noted
a slight drift to the left. He returned to the airport and made a normal
approach to the helipad followed by a normal flare. The aircraft then started to
drift to the left and would not correct with right cyclic; while trying to
correct the left drift with right cyclic, the cyclic became limited by his leg
and the confines of the cockpit. During an attempted go around, the pilot said
that his airspeed had decreased to zero, and his rotor RPM had dropped. He said
the helicopter began to descend and landed hard on the left forward skid.
Subsequently the helicopter rolled onto its left side.
The National Transportation Safety Board
determines the probable cause(s) of this accident as follows:
The pilot's failure to maintain main rotor
RPM resulting in an uncontrolled descent to a hard landing. A contributing
factor was his lack of experience in make and model of aircraft.
= = =
Accident occurred Thursday, March 01, 2007
in Camarillo, CA
Probable Cause Approval Date: 5/29/2007
Aircraft: Monocoupe 110, registration:
N18642
Injuries: 2 Minor.
The airplane ground looped and nosed over
while landing. The pilot said that during the landing rollout, directional
control of the airplane was lost and the left wing tip impacted the runway. The
left main landing gear then failed inboard, which resulted in a ground loop and
the airplane coming to rest inverted. The pilot said there were no mechanical
malfunctions or failures.
The National Transportation Safety Board
determines the probable cause(s) of this accident as follows:
The pilot's failure to maintain directional
control during the landing rollout that resulted in a ground loop.
= = =
Accident occurred Tuesday, July 18, 2006 in
Camarillo, CA
Probable Cause Approval Date: 10/31/2006
Aircraft: Cessna 177RG, registration: N34480
Injuries: 1 Uninjured.
The pilot made an inadvertent gear-up
landing, resulting in substantial damage to the airplane. While on final
approach, the pilot adjusted the propeller and the mixture for landing; he
failed to confirm the position of the landing gear. As the airplane was in the
landing flare, with the landing gear in the retracted position, the tower
controller instructed the pilot to abort the landing. The propeller struck the
runway surface before the pilot could recover, and the airplane subsequently
contacted the runway surface. Following the accident, an airplane mechanic at
the airport preformed a cursory exam of the landing gear system. He noted no
anomalies; the audible gear warning horn sounded when the respective circuit
breaker was pulled.
The National Transportation Safety Board
determines the probable cause(s) of this accident as follows:
the pilot's failure to extended the landing
gear and verify the proper landing gear configuration prior to landing,
resulting in a gear-up landing.
= = =
Accident occurred Sunday, June 11, 2006 in
Camarillo, CA
Probable Cause Approval Date: 4/25/2007
Aircraft: Cessna 152, registration: N452WC
Injuries: 1 Minor, 1 Uninjured.
The airplane experienced a loss of engine
power and nosed over during a forced landing. The airplane departed with full
fuel in both wing tanks. About 45 minutes into the training flight, the
certified flight instructor (CFI) began a demonstration of a simulated emergency
landing approach. The CFI configured the airplane for the maneuver, while the
student read the engine troubleshooting checklist aloud. As part of the maneuver
he pushed the throttle control knob forward every altitude loss of 500 feet in
an attempt to temporarily increase revolutions per minute (rpm) and "clear" the
throttle. The instructor said he had the carburetor heat control in the full on
position during the entire maneuver and it ended up in the off position during
the ground impact and nose over. While the airplane was about 1,500 feet msl and
on the simulated base leg of a traffic pattern, the CFI pushed the throttle
forward. The engine did not respond normally and sounded as
though it was winding up. After several
seconds, the engine quit and the propeller stopped. He attempted to restart the
engine by using the engine troubleshooting checklist, but it failed to respond.
The airplane touched down in a soft dirt field and nosed over, coming to rest
inverted. Personnel that recovered the wreckage shortly after the accident
stated that they found 15 to 20 gallons of fuel in the wing tanks and the
carburetor heat control in the off position. The outside air and dew point
temperatures around of the time of the accident were applied to an industry
Carburetor Icing Probability Chart. Both recorded temperatures were within the
"serious icing at glide power" portion of the chart. With the engine still
mounted in the airframe, investigators ran the engine for several minutes at
various rpm settings and noted no anomalies. No evidence was found of
pre-accident mechanical malfunctions during the examination of the engine and
airframe.
The National Transportation Safety Board
determines the probable cause(s) of this accident as follows:
a loss of engine power for undetermined
reasons. A factor was the soft terrain encountered during the emergency landing.
= = =
Accident occurred Tuesday, January 10, 2006
in Camarillo, CA
Probable Cause Approval Date: 5/30/2006
Aircraft: Huntington KIS, registration:
N506RJ
Injuries: 1 Serious.
The experimental airplane experienced a
partial loss of engine power in the takeoff initial climb, and collided with
obstacles and terrain during an emergency landing in an open field to the west
of the airport. The pilot stated that he was taking the newly constructed
airplane for its second flight. The engine that was installed in the airplane
was a automotive Subaru EJ20. He took off from runway 26 and was climbing at 90
mph. Everything seemed normal and then he noticed that his airspeed was 60 mph
and the engine sound had decreased. There were no pops or abnormal engine sounds
associated with the decrease in airspeed and the engine rpm was down at 1,700
instead of the normal 6,000. The pilot immediately manipulated the throttle to
ensure it was fully opened, he then turned the ignition switch off and on in an
attempt to reset the electronic engine control. Both actions failed to regain
full power of the engine. He notified the tower that he had lost
engine power. He decided to land in a field
that was off the end of the runway. He was flying at 60 mph and had a rate of
descent of a couple of hundred feet per minute. He made an forced landing into
the field and was assisted by emergency responders shortly afterwards. The pilot
said that the Subaru engine has a reduced power mode intended to operate the
engine at a substantially reduced power output if an engine problem was detected
by the engine electronic control system computer. He thinks that the engine
switched to this low power mode shortly after takeoff. The method he knew of to
correct this situation was to turn the ignition off then back on and this should
have cleared the fault and allowed the engine to resume normal power output. The
underlying reason for the engine going to the reduced power mode was not
determined.
The National Transportation Safety Board
determines the probable cause(s) of this accident as follows:
a partial loss of engine power due to the
engine's electronic control system reverting to a designed reduced power mode of
operation.
Camarillo Airpark Video: