Fallbrook Airport, Fallbrook, CA
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Area Accident History:
Accident occurred Thursday, December 06,
2007 in Fallbrook, CA
Probable Cause Approval Date: 2/28/2008
Aircraft: Piper PA-28-180, registration:
N44528
Injuries: 2 Uninjured.
While on approach for landing, the airplane
encountered a downdraft. The pilot attempted to arrest the sink rate by applying
full power; however, the airplane landed hard and short of the runway, damaging
surrounding vegetation and a runway edge light. After the hard landing the pilot
was able to get the airplane airborne again and he decided to return to his home
base airport. During the flight back to his home airport the left wheel and
strut fell from the airplane.
The National Transportation Safety Board
determines the probable cause(s) of this accident as follows:
The pilot's misjudged distance and altitude
that led to an undershoot and a failure to obtain the proper touchdown point.
= = =
Accident occurred Thursday, May 04, 2006 in
Fallbrook, CA
Probable Cause Approval Date: 4/25/2007
Aircraft: Bell 206B3, registration: N2763R
Injuries: 2 Minor.
The helicopter collided with trees following
a failure of the engine to transmission drive shaft. After finishing a final
rinse load for the agricultural spray operation, the pilots began the short
return flight back to a trailer. While maneuvering about 20 feet above ground
level (agl), and about 5 feet above the treetops, the helicopter made an
uncommanded yaw and settled into the trees. A post accident examination revealed
that the engine to transmission drive shaft (short shaft) was separated at the
forward coupling flange, adjacent to the transmission. Investigators removed the
rust-covered engine to transmission drive shaft forward coupling from the gear.
The retainer ring, packing seal, and drive shaft coupling seal were not attached
to the coupling and dangling loosely on the drive shaft tube. A visual
examination of the internal coupling revealed that grease retainer plate had a
shiny polished appearance from the gear sprocket making repetitive
contact with its surface. The engine to
transmission drive shaft forward gear sprocket teeth were not present, as a
result of overheating and persistent contact, which had worn them smooth. On the
face of the gear sprocket there was a semicircular indentation that had the
shape and dimension consistent with that of a partial impression of the spring
that is normally inside the coupling. Pieces of the spring were found deformed
in the aft coupling housing. There was no evidence of grease in the forward
coupling, and the aft coupling contained grease that was dirty and black. The
operator's component card record for the engine to transmission drive shaft
indicated that it was last inspected about 2 months prior to the accident at
which time a mechanic repacked the couplings with grease. The helicopter's
applicable Maintenance Manual indicated that every 600-hour or 12-month period
(whichever occurs first) the main drive shaft component should be
inspected.
The National Transportation Safety Board
determines the probable cause(s) of this accident as follows:
Failure of the engine to transmission drive
shaft forward coupling due to overheating from lack of lubrication. The cause of
the lack of lubrication was a result of improper maintenance. A factor was the
trees.
= = =
Accident occurred Monday, January 09, 2006
in Fallbrook, CA
Probable Cause Approval Date: 4/25/2006
Aircraft: Bellanca 7KCAB, registration:
N36382
Injuries: 1 Minor.
The airplane veered off the runway and
collided with trees while performing a touch-and-go takeoff and landing. The
student pilot said that airplane bounced slightly and he pulled back on the
control stick to cushion the second touchdown. After the airplane settled onto
the runway, a gust of wind lifted the right wing. The left wing was pushed into
the ground, rotating the airplane to the right. At that point the airplane was
traveling towards parked airplanes in the transient area. The student pilot
attempted to correct back to the runway with the use of full left rudder and
left brake; however, his flight control inputs did not affect the direction of
travel. He applied full throttle to get airborne again and steer the airplane
back towards the runway, but collided with trees on the east side of the
airport. Reported winds in the area were from 010 to 030 degrees between 4 to 10
knots.
The National Transportation Safety Board
determines the probable cause(s) of this accident as follows:
the student pilot's inadequate compensation
for a crosswind condition and his failure to maintain directional control.
= = =
Accident occurred Friday, July 29, 2005 in
Fallbrook, CA
Probable Cause Approval Date: 7/31/2006
Aircraft: Beech B23, registration: N6121N
Injuries: 1 Minor.
The airplane veered off the runway and
collided with an unoccupied parked airplane following the pilot's loss of
directional control during the landing rollout. The pilot's approach to the
airport was normal, and the airplane touched down without mishap near the
centerline of runway 18. The wind was from 180 degrees, at 8 knots. The pilot
said the airplane swerved left after he applied brakes and he could not regain
control. Left and right tire skid marks were observed on the tarmac leading from
the runway to the accident airplane. No evidence was found or any mechanical
malfunction with the airplane's brakes, wheels, or tires.
The National Transportation Safety Board
determines the probable cause(s) of this accident as follows:
The pilot's failure to maintain directional
control during the landing rollout.
= = =
Accident occurred Saturday, March 11, 2000
in Fallbrook, CA
Probable Cause Approval Date: 11/25/2003
Aircraft: Cessna 182Q, registration: N95996
Injuries: 1 Fatal, 1 Serious.
A witness observed the airplane taxi from
the pilot's hangar to the runway without conducting an engine run-up. Shortly
after takeoff, the engine lost power. Witnesses reported that the airplane
cleared utility lines and then pitched nose down, impacting terrain in a nose
low attitude. The passenger stated that she didn't think that the private pilot
performed an engine run-up prior to takeoff. She added that after the engine
lost power, the pilot reached down to the lower section of the center column
area and turned something. The fuel selector valve is located on the bottom of
the center control column and is operated by manually rotating the selector
valve handle to one of the four positions; OFF, LEFT, BOTH, and RIGHT. The fuel
selector valve was found in the left fuel tank position. Fuel was found in the
fuel line immediately upstream of the boost pump, however, no fuel was found
between the gascolator and the boost pump. The airplane had been
modified by STC for a Continental IO-550
engine; part of the installation involved installing a 1-quart capacity header
tank between the selector and fuel control unit. The engine was operated on a
test stand and no anomalies were noted that would have prevented its operation.
One of the witnesses was also an acquaintance of the pilot and reported that the
pilot was in the habit of turning the fuel selector to the off position when the
he hangared his aircraft. This was due to instances in the past in which fuel
had leaked on his hangar floor when the fuel selector had not been turned off.
He added that the pilot experienced a loss of engine power while taxiing in the
past due to the fuel selector being in the off position. The Preflight
Inspection, Before Starting Engine, and Before Takeoff checklists instruct the
pilot to place the fuel selector valve in the on or both position. Toxicological
tests on the pilot were positive for paroxetine, and
verapamil. Paroxetine is a prescription
antidepressant drug and verapamil is a prescription medication for high blood
pressure. The paroxetine is not approved by the FAA for use during flight;
however current medical literature shows the drug does not appear to have
adverse performance effects when taken in therapeutic dosages. The subtle
effects of higher than normal doses have not been systematically investigated,
though symptoms of over dosages have been reported to include sedation and
dizziness. The pilot did not report the use of the aforementioned medications on
his last application for an airman medical certificate.
The National Transportation Safety Board
determines the probable cause(s) of this accident as follows:
the loss of engine power resulting from fuel
starvation due to the pilot's inadequate pre-flight inspection, inadequate
performance of the pre-takeoff checklist, and failure to ensure that the fuel
selector was properly positioned prior to takeoff. Also causal was the pilot's
failure to maintain an adequate airspeed while attempting to clear a power line
during the ensuing forced landing, which resulted in an inadvertent stall.
Fallbrook
Airport Approach /
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