Airport
Area Accident History:Accident occurred Wednesday, July 29, 2009 in
Firebaugh, CA
Aircraft: AIR TRACTOR AT-301, registration: N23189
Injuries: 1 Uninjured.
This is preliminary information, subject to change, and may contain errors. Any
errors in this report will be corrected when the final report has been
completed.
On July 29, 2009, about 0415 Pacific daylight time, an Air Tractor Inc. AT-301,
N23189, sustained substantial damage following a forced landing to a field about
5 nautical miles northwest of Firebaugh, California. The certificated commercial
pilot was not injured. Visual meteorological conditions prevailed for the aerial
application flight, which was conducted in accordance with 14 Code of Federal
Regulations (CFR) Part 137, and a flight plan was not filed. The flight departed
from a private airstrip about 4 miles east of Dos Palos, California, at 0410.
In a telephone conversation with the NTSB investigator-in-charge (IIC), the
pilot reported that as he was coming into the field the engine lost power
without warning. The pilot further reported that at this point he elected to
land straight ahead in the alfalfa field he was spraying. The pilot stated that
the landing was uneventful until the airplane collided with a ditch, which
resulted in the airplane nosing over. The empennage sustained substantial damage
due to impact forces.
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On March 23, 2009, about 1800 Pacific daylight time, a Piper PA-28-181, N1857H,
experienced a loss of engine power followed by a forced-landing in a field short
of Firebaugh Airport, Firebaugh, California. The pilot was operating the
airplane under the provisions of 14 Code of Federal Regulations Part 91. The
certificated private pilot was not injured. The airplane sustained substantial
damage to the left wing spar. The personal flight departed Palm Springs
International Airport, Palm Springs, California, at 1400, with a planned
destination of Reid-Hillview Airport, San Jose, California. Visual
meteorological conditions prevailed, and no flight plan had been filed.
The pilot reported departing Palm Springs with about 45 gallons of fuel onboard.
She initiated a northbound climb to an altitude of 10,500 feet and then changed
course to the northwest. About 3 1/2 hours into the flight, she checked the fuel
gauges, and observed slightly less than 5 gallons remaining in the right tank
and less than 10 gallons in the left tank. The fuel selector was set to the
right tank, and she presumed that there was enough fuel remaining for about 1
hour 10 minutes of flight.
About 15 minutes later, the engine stopped producing power. She checked the fuel
gauges, and observed the right needle was indicating zero fuel. She switched to
the left tank, and the engine regained power.
The pilot then diverted to the northeast with the intention of landing at
Firebaugh Airport. According to a statement made to the Fresno County Sheriff,
she was initially unable to locate the airport, and circled around the city of
Firebaugh. She then located the airport, and during the landing attempt the
engine lost power again. The pilot force-landed in a plowed field.
An FAA Inspector responded to the accident site. He examined the airplane, and
reported that both fuel tanks were intact and absent of fuel. The inspector did
not observe fuel leaks on the external surfaces of the airplane. Recovery
personnel drained approximately 32 ounces of fuel from the airplane, and
observed no indications of fuel leakage. Additionally, all fuel lines within the
engine compartment were intact.
The pilot stated that she was certain she leaned the fuel mixture during the
flight. However, she further reported that she often had difficulty accurately
adjusting the fuel mixture on the accident airplane type, due to its mixture
lever. She stated that she was more familiar, and comfortable, adjusting the
mixture on an airplane equipped with a Vernier mixture control.
The accident location was approximately 71 miles south of Reid-Hillview Airport.
The pilot reported encountering 35 knot headwinds during the flight.
In a written statement the pilot reported that the accident could have been
prevented with, "better planning/execution."
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On February 18, 2005, at 0811 Pacific standard time, an Ayres S2R, N4009M,
impacted soft muddy terrain shortly after departing Firebaugh Airport,
Firebaugh, California. Vance Ag was operating the airplane under the provisions
of 14 CFR Part 137 as a local aerial application flight. The commercial pilot,
the sole occupant, sustained fatal injuries; the airplane sustained substantial
damage. Visual meteorological conditions prevailed, and a flight plan had not
been filed.
According to the operator, the accident flight was to be the pilot's fourth
flight of the day in that airplane. The pilot had landed just prior to the
accident, and subsequently departed with a full load of Urea fertilizer.
During a telephone conversation with a National Transportation Safety Board
investigator, a witness stated that while exiting his office on the north end of
the airport, he observed the accident airplane depart the runway. After the
airplane climbed above several transmission wires, the engine made two "tszzz"
whirling sounds, and subsequently became silent. The airplane pitched down in a
nose-low configuration and dove toward terrain. The pilot initially egressed the
airplane, but succumbed to his injuries about 30 minutes thereafter.
A Federal Aviation Administration (FAA) inspector examined the airplane after
the accident occurred. He stated that the propeller blades did not exhibit any
high energy impact signatures, and remained straight. While conducting an
examination of the airplane he noted that the seatbelt was separated.
AIRCRAFT INFORMATION
The airplane was an Ayres S2R-T34, serial number 6012. A review of the
airplane's logbooks revealed that the airframe had undergone a 100-hour
inspection on August 26, 2004, at a total time of 11,193.4 hours. The airplane
was powered by a Pratt & Whitney PT6A-34AG turboprop engine (serial number
56561) that had accumulated an estimated total time of 17, 215 hours since
manufacture (May 1979). A review of the engine logbooks revealed that the last
engine overhaul was performed on August 24, 2003, at the airplane's Hobbs time
of 9,701.1 hours. At that time the compressor turbine (CT) disk was installed
(serial number 1M560) with 10,012 cycles already consumed (a notation stated
5,988 cycles remained ). The engine's most recent inspection occurred on
December 30, 2004. The entry indicated that the mechanic preformed a hot section
inspection at which time the CT disk was reinstalled with 3,595 cycles
remaining.
The airplane was configured with one pilot seat located directly in the middle
of the cockpit. The control stick is oriented in front of the seat, between the
pilot's legs.
A representative for the airplane manufacturer stated that the seat and
seatbelts/shoulder harnesses involved in the accident were not tested by Thrush
Aircraft, Inc., or its predecessors, because the seat was qualified to Technical
Standard Order (TSO) C39 and the belts to TSO C22F, which occurred prior to
Thrush Aircraft's involvement and testing of restraint systems.
As a reference, the representative further stated that the installation of seats
used before the ones installed on the accident airplane were tested by Thrush
Aircraft, Inc., to loads specified by Civil Aviation Regulation (CAR) 3.186,
with CAR 3.190 fitting factors and CAM 8 loads. This corresponds to the
installation being tested in the up direction to 3.0 x 1.33 = 3.99g, in the down
direction to 3.8 x 1.33 x 1.5 = 7.58g, in the side direction to 3.0g, and in the
forward direction to 9.0 x 1.33 = 11.97g. The representative further stated that
the shoulder harnesses were introduced after the original certification, and
their installation structure was analyzed for a 190-pound person to a forward
g-load of 9.0.
MEDICAL AND PATHOLOGICAL INFORMATION
The Fresno County Coroner performed an autopsy on the pilot. A review of the
autopsy report disclosed that there were no visible external injuries to the
head or neck area of the pilot. He sustained injuries to his abdomen with the
report noting an abrasion (4 inches by 0.5 inches) and contusion (3.5 inches by
1.5 inches) on the right side. It was also noted that the sternum was fractured
at its upper 1/3, with extravasations of blood over his chest area. Blood was
also located in the chest cavity. The pilot's spleen was severely lacerated.
The autopsy report additionally noted significant contusions on the pilot's
legs, around the knee and thigh area. The pelvic bones were intact. The forensic
pathologist who preformed the autopsy opined that the cause of death was, "chest
and abdominal trauma due to blunt impact." The Fresno County's toxicological
testing results were positive for Delta-9-THC at the level noted of 45 ng/ml and
9-Carboxy-11-nor-Delta-9 at a level of 720 ng/ml.
The FAA Toxicology and Accident Research Laboratory additionally performed
toxicological testing of specimens of the pilot. The results of analysis of the
pilot's specimens were negative for ethanol, carbon monoxide, and cyanide. The
testing found tetrahydrocannabinol (marihuana) in both the blood and liver
specimens at levels of 0.0075 (ug/ml, ug/g) and 0.023 (ug/ml, ug/g),
respectively. It additionally revealed tetrahydrocannabinol carboxylic acid in
the blood and liver specimens at levels of 0.1219 (ug/ml, ug/g) and 0.1626 (ug/ml,
ug/g), respectively.
TEST AND RESEARCH
Engine Examination.
The engine was shipped to Pratt & Whitney Canada for examination. Under the
auspices of a Transportation Safety Board of Canada investigator, the engine was
disassembled at the Montreal facilities on May 10 and 11, 2005.
The compressor first stage rotor appeared intact, showing no indications of
distress. The compressor turbine (CT) blades were all missing material at the
tips, varying in heights. One blade was fractured below the fir tree area and
was significantly shorter than the other blades. The CT shroud displayed molten
material with gouging on the sides.
The power turbine (PT) guide vane airfoil leading edges displayed nicks and
gouge marks consistent with contact from separated compressor turbine blade
debris. A majority of the PT blades were fractured at varying heights and
displayed characteristics of contact with separated CT blade debris and contact
with the PT shroud. The remaining blades and PT guide vane displayed
circumferential rubbing; the external housing had been deformed, which appeared
to be a result of impact damage.
Blade Examination.
Personnel from the Safety Board Materials Laboratory examined the fracture face
of the subject CT blade. The fracture surface appeared smooth with a curving
boundary, typical of fatigue. Near the fatigue origin, no surface damage was
observed and no material anomalies were visible on the fracture surface. The
facture was located above the region of fretting noted in the fir tree root.
The manufacturer of the blade could not be positively established from the
limited portion of the blade that remained. The part number (T-102401-100A) on
other blades in the set indicated that they were manufactured by Turbo Products,
a Division of Doncasters, Inc., who are the sole Parts Manufacturer Approval
(PMA) manufacturer for the blades. The remaining blades were all machined with
heat code identification of 13CBF. Personnel from the Safety Board Materials
Laboratory further reported that the chemistry of the fractured blade appeared
to be consistent with the PMA specified alloy and not to the material Pratt &
Whitney Canada utilizes for manufacturer. A review of the Safety Borad database
revealed an instance of a very similar failure on a Pratt & Whitney Canada
manufactured CT blade (see accident number SEA00LA160).
A representative from the blade manufacturer stated that the heat code on the
surrounding blades corresponded to a batch of blades manufactured in mid 2004.
He stated that the blades were shipped from their facility between August 4 and
September 14, 2004.
Seat Belt Examination.
The separated seatbelt was sent to the FAA Civil Aerospace Medical Institute
Biodyamics Lab for examination. The seatbelt, a four-point restraint system,
consisted of a 3-inch wide lap belt and dual 2-inch wide shoulder straps. The
shoulder straps had their own respective inertia reels and connected to the lap
belt at a center latch. The TSO tags on both straps were faded and illegible.
The right lap belt was faded with different hues displaying evidence of
environmental exposure. The webbing was frayed at the adjuster bar and the metal
latch tongue had markings that the inspector stated was consistent with heavy
loading. The upper portion of the belt was disintegrated from the tongue to 2
inches down the length of the belt. The belt length showed minor fraying along
the bottom edge at the adjuster bar and the latch tongue. The left lap belt was
torn where the webbing passed through the adjustment mechanism. The inspector
stated that the pattern of the webbing tear indicated that the tear initiated at
the top edge where it passed over the bar.
The FAA's lab inspector stated that minor fraying of the lower edge of the lap
belt's webbing was consistent with normal wear. The severe fraying
(disintegration) of the upper portion of the right belt and the separation of
the webbing at the adjuster on the left lap belt is consistent with heavy
loading during the accident sequence. He further stated that the entire belt
appeared to be contaminated with chemicals. The reduction in webbing strength
due to chemical and normal ultra violet (UV) light exposure was unknown. There
was not enough section of undamaged webbing to perform a static strength test.
A review of the airframe logbooks revealed that on April 4, 1995, a mechanic
made a notation specifically notating that the seat belts were inspected during
his 100-hour inspection; the Hobbs time was entered to be 1,722.8 hours.
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