General William J Fox Airfield, Lancaster, CA
Location:
History:
General William J Fox Airfield Today:
Airport
Services and Amenities:
Special Events:
Airport Area Accident History:
Accident occurred Wednesday, January 10, 2007 in
Lancaster, CA
Probable Cause Approval Date: 6/27/2007
Aircraft: Cessna 172S, registration: N534SP
Injuries: 1 Uninjured.
The student pilot stated that wake turbulence was
encountered during the takeoff roll, directional
control was lost, and the airplane nosed-over after
impacting a berm off the runway surface. A larger,
twin-engine jet aircraft landed long about 2 minutes
prior to the accident. The student pilot then
landed, stopped, and began his takeoff roll. During
the takeoff roll, the airplane began to veer to the
left. The pilot attempted to realign the airplane on
the centerline by applying right rudder and right
brake, at which time the airplane veered sharply to
the left in a skidding motion. The airplane impacted
a berm and nosed-over. The FAA accident coordinator
stated that there were no pre-impact mechanical
anomalies with the airplane. Winds were calm at the
time of the accident.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The reason for the loss of directional control was
undetermined.
===
Accident occurred Monday, January 09, 2006 in
Lancaster, CA
Probable Cause Approval Date: 9/27/2007
Aircraft: Cirrus Design Corp. SR20, registration:
N526CD
Injuries: 2 Fatal.
While simulating an engine failure on climb-out, the
airplane was observed to enter a left teardrop
maneuver as it attempted to return to the airport.
During the turn, the airplane stalled, entered a
spin, and impacted level terrain 1 nautical mile
northeast of the departure end of runway 06. The
reported winds were 060 degrees at 15 knots.
According to the air traffic controller working the
local control position, after completing several
touch-and-go landings on runway 06, the instructor
requested the first of two teardrop return to runway
engine-out maneuvers. During the first one, the
airplane made a left teardrop 180-degree turn as it
attempted to land on runway 24. During the turn, the
airplane appeared to lose a significant amount of
altitude. The controller stated that the airplane
recovered prior to landing, and then executed a
go-around to reenter the traffic pattern. During the
second attempt, the airplane again entered a
teardrop turn to the
left and then "spin to the ground." An examination
of the wreckage revealed that the airplane impacted
the terrain in a 70-degree nose down, left wing low
attitude. All flight control surfaces, engine,
propeller, and Cirrus Airframe Parachute System
(CAPS) components were located at the site. The
engine and propeller were embedded in the ground
approximately 2 feet, and all three propeller blades
exhibited rotational scoring. Recorded data was
retrieved from the Avidyne Primary Flight Display
(PFD) and Multi-Function Display (MFD). The data log
retrieved for the accident flight included data from
a time stamp of 12:17:36 to 13:32:00 on January 9,
2006. The next scheduled data-logging event would
have been at 13:33:00; however, the unit operation
ceased prior to reaching the next recording point.
At the last data sampling point, the engine rpm
(revolutions per minute) was at 2,680 rpm, the
engine manifold pressure was 27.5 inches, and the
airplane
electrical bus voltage was 27.5 volts. The recorded
data did not show any engine or system anomalies.
The information from the download of the MFD was
consistent with the visual information provided by
witnesses.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The student pilot's failure to maintain an adequate
airspeed while maneuvering, and, the flight
instructor's inadequate supervision of the flight. A
factor in the accident was the strong tailwind
encountered as the airplane turned from an upwind to
a downwind during the teardrop maneuver.
===
Accident occurred Tuesday, December 27, 2005 in
Lancaster, CA
Probable Cause Approval Date: 4/25/2006
Aircraft: SOCATA TBM 700, registration: N198X
Injuries: 2 Minor.
The airplane stalled on short final approach, and it
impacted the ground. The purpose of the flight was
for the student to receive dual flight instruction
to become more acquainted with the airplane's
handling characteristics. The student met with his
certified flight instructor and received a briefing
regarding the upcoming lesson involving, in part,
takeoff and landing practice. The instructor
directed his student to perform a simulated engine
out approach, and engine power was reduced as the
airplane glided toward the airport. The student
entered a close in downwind approach and, at the
direction of the instructor, then performed a left
circling turn onto the base and final approach legs.
The landing gear was lowered, and the student
questioned the instructor regarding whether they
could glide all the way to the runway. The
instructor advised his student to maintain 90 knots
airspeed. During the descent, as the airplane turned
from the close in base
leg onto the final approach leg, the instructor told
his student "don't bank." The student rolled the
wings level. Immediately thereafter, the left bank
began a second time and the instructor again said,
"Don't bank." The student replied, "I'm not." The
instructor applied engine power and right rudder to
reduce the left bank. The airplane stopped rolling
left, and then rolled into a right bank, whereupon
the right wing impacted the ground. At no time did
the instructor direct his student to release the
airplane's flight controls.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The student's failure to maintain adequate airspeed,
and the instructor's inadequate supervision and
delayed remedial action, which resulted in a
stall/mush.
===
Accident occurred Wednesday, August 10, 2005 in
Lancaster, CA
Probable Cause Approval Date: 4/25/2007
Aircraft: San Joaquin Helicopters OH-58A+,
registration: N177SJ
Injuries: 1 Fatal.
Following a loss of engine power, the helicopter
impacted the ground during the application of
chemicals to an agricultural field. Post accident
examination of the engine showed that the power
turbine to pinion gear coupling had fractured.
Metallurgical examination of the affected components
showed that the coupling failed in fatigue, which
effectively separated the engine from the main rotor
gearbox. The fatigue was the result of a misaligned
power turbine outer shaft, where the axis of the
turbine shaft was angled slightly relative to the
coupling and pinion axes. The turbine section had
been removed from another engine due to metal
contamination. The turbine section was repaired and
subsequently installed on the accident helicopter on
August 11, 2004, where it operated for 770.3 hours
prior to the accident. Weight and balance
calculations showed that the helicopter was in
excess of its certificated maximum gross weight by
174 pounds.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pinion to turbine shaft coupling failed in
fatigue due to a misaligned turbine shaft, which
resulted in a loss of engine power.
===
Accident occurred Sunday, September 12, 2004 in
Lancaster, CA
Probable Cause Approval Date: 12/3/2004
Aircraft: Smith S-51D, registration: N51VS
Injuries: 1 Uninjured.
The airplane impacted the runway in a 3-point
attitude, the main landing gear forks fractured, and
the airplane skidded off the right side of the
runway. The pilot/owner/builder had just recently
completed fabricating the airplane, and the purpose
of the flight was to develop emergency procedures
for engine out landings. The pilot configured the
airplane with the landing gear down, flaps up, and
the engine at 3,800 rpm (1,784 propeller rpm). He
would perform the maneuver at 110 knots. The first
attempt left him rolling onto final 1/4 mile short
of the runway, so he added power and did a
touch-and-go. During the second attempt the pilot
overshot the runway extended centerline and executed
a go-around. On the third attempt the pilot had the
airplane on final, at 200 feet agl, on the runway
extended centerline, and about 100 knots. He pulled
the stick back to arrest the sink rate. He noted
that the angle of attack (AOA) indicator was reading
three red dots
(indicating that the airplane was within 10 percent
of stalling), and the airplane impacted the runway
in a 3-point attitude. The main landing gear forks
fractured, and the airplane skidded off the right
side of the runway, traveling some 600 feet beyond
the impact point.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's misjudged landing flare, failure to
correct the descent rate, and failure to execute a
go-around during an unstablized landing approach.
===
Accident occurred Wednesday, June 23, 2004 in
Lancaster, CA
Probable Cause Approval Date: 12/28/2004
Aircraft: Bell 206B, registration: N305FD
Injuries: 2 Minor.
The helicopter landed hard and rolled on its side
during a practice autorotation. The CFI and
pilot-undergoing-instruction (PUI) were practicing a
180-degree autorotation. The PUI rolled out onto
final at 400 feet agl. The PUI said that about 70
feet agl he leveled the helicopter, rolled in
throttle, and started his flare. About 50 feet agl,
he leveled in the flare because the helicopter "did
not feel like it was building energy" and was not as
effective in the flare. The rotor rpm was at 100
percent. He noted that there seemed to be not enough
engine power to recover. He leveled the aircraft to
get out of the flare and raised the collective. The
low rotor horn sounded shortly after. The helicopter
landed hard, bounced, spun around, hit the ground
again, and rolled over on its right side. The Los
Angeles City Fire Department "flare autorotations"
procedure states "At approximately 75 feet from the
ground, you begin your flare by applying a smooth
pressure on the cyclic, flaring the ship at the
right altitude and leveling the ship from a flare
require quick but smooth movement of the
cyclic...You will lost some altitude coming out of
the flare but the ship should be level by the time
you reach 10 feet." An engine teardown was
conducted, with no anomalies found. The fuel control
and governor bench tested to specifications.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's misjudged autorotative flare and the
flight instructor's delayed remedial action and
inadequate supervision of the flight.
===
Accident occurred Friday, May 14, 2004 in Lancaster,
CA
Probable Cause Approval Date: 12/28/2004
Aircraft: Downer Bellanca 14-19-2, registration:
N7658B
Injuries: 2 Minor.
The airplane impacted sagebrush during a forced
landing following a loss of engine power. The
commercial pilot reported he was in cruise flight at
1,000 feet above the ground when the engine lost
power. The pilot reported the loss of power was "in
a manner indicative of fuel starvation." The pilot
switched fuel tanks from the auxiliary fuel tank to
the right main fuel tank and attempted an engine
restart with the wobble pump. The pilot obtained an
engine surge, but no power. He switched to the left
main fuel tank and utilized the wobble pump again,
to no avail. The pilot then set up for the forced
landing in desert terrain. Post-accident examination
of the aircraft revealed there was no fuel present
in the auxiliary fuel tank, while the left and right
main fuel tanks had 10 and 15 gallons of fuel,
respectively. No fuel was present in the gascolator,
the carburetor, and any of the fuel lines forward of
the firewall. The aircraft's operation manual
indicates that the auxiliary fuel tank should not be
completely emptied in flight because it will result
in air being pumped into the fuel line.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's fuel mismanagement by his failure to
follow the recommended procedures for operation of
the auxiliary fuel tank, which resulted in fuel
starvation and loss of engine power during cruise
flight.
===
Accident occurred Thursday, October 16, 2003 in
Lancaster, CA
Probable Cause Approval Date: 10/31/2006
Aircraft: Beech A36, registration: N700TT
Injuries: 1 Uninjured.
The airplane collided with power lines during an
off-airport forced landing following a loss of
engine power. While in cruise at 10,500 feet, the
pilot heard a bang, and the engine lost power. He
declared an emergency, and attempted to glide to a
nearby airport; however, he was unable to make it to
the runway. The airplane collided with power lines
and fell to the ground about 4 miles west of the
airport. The N1 and N2 shafting systems were bound
up and would not move. The upper magnetic chip
detector was free of metal, but it did contain coke.
There was slight varnishing of the anode and
cathode. The lower magnetic chip detector contained
a substantial amount of metallic particles,
subsequently identified as material from the No. 5
bearing. The particles did bridge the gap from anode
to cathode. A detailed examination of the engine
determined that three sections of the first stage
turbine wheel separated. The stub shaft also
fractured and separated, and
a portion of the fractured tie bolt remained in the
wheel. Metallurgical examination of the first and
second stage turbine wheels found evidence of gamma
prime solutioning and localized melting of the
second stage turbine wheel airfoil tips, indicating
temperature exposures above 2,100 degrees Farenheit,
a temperature range outside the normal operating
envelope of these wheels. This exposure to elevated
temperatures resulted in rim separation due to
thermal fatigue initiating at the rim followed by
accelerated interdendritic creep crack growth. No
evidence of an oil fire was associated with the
first stage wheel separation. The composition,
hardness, and microstructure of the first stage
turbine wheel were as required by the engineering
drawing. The No. 5 bearing exhibited heat distress,
but the cause of this could not be conclusively
determined. According to Rolls-Royce Allison, the
internal evidence of excessive thermal damage to the
first and second
stage turbine wheels was consistent with prior
examples of known hot starts.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
A loss of engine power due to thermal fatigue
failure of the first stage turbine wheel resulting
in release of a section of its rim. The thermal
fatigue was due to the engine exceeding its
temperature limits during one or more start cycles.
===
Accident occurred Thursday, January 30, 2003 in
LANCASTER, CA
Probable Cause Approval Date: 7/31/2006
Aircraft: Beech D95A, registration: N5639S
Injuries: 2 Fatal.
The airplane collided with a hangar during a
go-around. The flight crew entered the traffic
pattern and completed one touch-and-go landing. The
crew requested, and the controller cleared them, for
a simulated single engine full stop landing on
runway 24. The controller thought that the
touch-and-go approach and landing was unremarkable
and perfectly normal. On the single engine full stop
approach, he thought that the airplane made a short
approach with the wings rocking back and fourth. The
airplane looked like it was low and could possibly
land short of the runway. As the airplane approached
the end of the runway, it began to veer to the left
(from the flight crew's perspective). The controller
said it appeared to be headed directly for the
control tower as it continued to drift left. The
airplane stayed low to the ground and the controller
had the impression that the flight crew was
attempting to climb. The wing lights were
continuously rocking back
and fourth as the airplane continued to drift left
and it crossed the dirt infield and a taxiway while
still airborne. The bank angle then increased
sharply to the left, and the airplane disappeared
behind some hangars. The controller estimated that
the airplane was 1,500 feet from the approach end of
the runway when he observed a fireball and alerted
rescue crews. The instructor pilot's autopsy noted
undiagnosed lung cancer that had metastasized to his
brain. The brain showed evidence of severe swelling,
with disruption of the normal brain structure. The
instructor pilot had been prescribed a pain
medication (tramadol), which was found in the
instructor pilot's blood at a level consistent with
regular use at least at the dose prescribed. The
medication is known to increase the risk for
seizures, particularly in patients with other
potential seizure risks. The effects of the brain
swelling and the medication likely produced seizure
activity in the
instructor which could have significantly interfered
with the aircraft controls and made it difficult or
impossible for the student to have adequately
controlled the aircraft.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
a loss of aircraft control due to the instructor
pilot's incapacitation by seizure activity as a
result of his undiagnosed cancer, and his use of a
medication that can increase seizure risk.
===
Accident occurred Tuesday, April 23, 2002 in
LANCASTER, CA
Probable Cause Approval Date: 6/2/2004
Aircraft: Cessna 340A, registration: N6304X
Injuries: 1 Uninjured.
Following a normal approach and landing, the right
main landing gear collapsed during the landing
rollout. Post accident examination revealed the
landing gear selector was in the down position and
the landing gear microswitches were dirty, but not
cracked or broken. After maintenance personnel
replaced the microswitches, the landing gear
functioned properly.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The collapse of the right main landing gear as a
result of a malfunctioning microswitch.
===
Accident occurred Wednesday, April 18, 2001 in
Lancaster, CA
Probable Cause Approval Date: 11/28/2001
Aircraft: Cessna 172B, registration: N4672L
Injuries: 2 Serious, 1 Minor.
The pilot attempted to climb the airplane into
rising terrain in a box canyon. Surface wind at 18
knots with gusts to 24 knots formed a downdraft on
the lee side of a ridge forming one side of the
canyon. The density altiude was 5,000 feet. The
pilot reported the aircraft "experienced involuntary
descent" and despite full engine power the aircraft
was "unable to gain/maintain altiude resulting in
[a] forced landing." He also reported he "put in a
little flap to keep from settling." No mechanical
anomalies were found with the airplane.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's delay reversing course while flying
toward rising terrain in a box canyon. Factors in
the accident included a downdraft on the lee side of
a ridge forming the box canyon, high density
altitude, and the pilot's improper use of flaps.
===
Accident occurred Tuesday, December 12, 2000 in
Lancaster, CA
Probable Cause Approval Date: 11/25/2003
Aircraft: Cessna 182P, registration: N182ER
Injuries: 1 Fatal.
The commercial pilot lost control of the single
engine airplane during a rapid descent to the
arrival airport, and impacted the ground in a near
vertical attitude at very high speed. The pilot
reported he was 7 or 8 miles from the airport at
8,500 feet msl, and was inbound for landing. The
controller asked the pilot if he would be able to
descend from his position. The pilot answered,
"Yeah, if I could do right traffic, I'll go into a
imitation of a rock, see what I can do." The
controller told the pilot to enter a left downwind
leg at a midfield position, and issued the wind
conditions, which were reported as 270 degrees at 25
knots. Several witnesses, within a mile of the
accident site, reported seeing the airplane as being
in a steep, nose down attitude at a rapidly
increasing rate of descent. The airplane maintained
a perpendicular, nose down attitude until they lost
sight of the airplane behind low scrub brush. About
the same time they lost sight,
they reported seeing a dust cloud rise in the same
vicinity. The dust cloud quickly dissipated in the
gusting surface winds. The airplane's mode C radar
data depicted the airplane descending at a rate of
5,500 feet per minute between the last two radar
returns, which were spaced 12 seconds apart. The
airplane's last radar return was depicted as 4,900
feet msl (2,545 feet above the ground). Co-workers
described the following procedure used by the mishap
pilot to lose altitude quickly: reduce power and
slow airplane to 120 knots; position propeller
control full forward; allow the engine temperatures
to normalize; and trim airplane nose down to achieve
an indicated airspeed near Vne (redline - Never
Exceed Speed; 176 knots). It was reported the pilot
learned this from other pilots who took parachutists
to altitude. No pre-accident anomalies were noted
with the airframe and engine during the examination.
The main wings and all fixed and movable primary and
secondary control surfaces were accounted for at the
impact site. No evidence was found to support a
physiological incapacitation. Investigators
considered the possibility of some combination of
airplane attitude and speed aerodynamically blanking
the empennage surfaces; however, no evidence to
support such a conclusion was found.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's in-flight loss of control for
undetermined reasons.
===
Accident occurred Saturday, July 15, 2000 in
LANCASTER, CA
Probable Cause Approval Date: 11/1/2001
Aircraft: Piper PA-22-160, registration: N8768D
Injuries: 2 Minor.
The pilot was on approach to the dirt airstrip where
he based his airplane when he encountered wind
gusts, which he said buffeted him around and caused
a loss of lift. The airplane came into contact with
power lines, which were about 30 feet agl. The
airplane descended nose first and struck the ground.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's inadequate compensation for gusty winds
conditions that resulted in the collision with a
power line during final approach.
===
Accident occurred Wednesday, May 31, 2000 in
LANCASTER, CA
Probable Cause Approval Date: 7/30/2001
Aircraft: Hilyard DRAGONFLY, registration: N22EX
Injuries: 1 Uninjured.
During a series of high-speed runway taxi tests, a
gust of wind caused the airplane to become airborne
and veer to the right of centerline. Due to the
insufficient remaining runway, the pilot added full
power and continued the initial climb out within the
traffic pattern. On the landing flare, a gust of
wind raised the nose of the airplane reducing the
airspeed, and the canard pitch authority became
inadequate. The airplane struck the runway with the
canard tip mounted wheels, porpoised three times,
then departed the runway and came to rest nose down.
Recorded winds were from 240 degrees at 12 knots
gusting to 14 knots.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's failure to maintain adequate airspeed
while attempting to land in gusty wind conditions
leading to an inadvertent stall/mush, which resulted
in a porpoise and subsequent loss of directional
control.
General William J Fox
Airfield Approach / Landing: