Oxnard Airport, Oxnard, CA

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Airport Area Accident History:
Accident occurred Saturday, August 09, 2008 in Oxnard, CA
Aircraft: Smith Stewart S51D, registration: N51VS
Injuries: 1 Serious.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

On August 9, 2008, about 1514 Pacific daylight time, a Smith Stewart S51D, amateur built experimental airplane, N51VS, experienced a loss of engine power while on approach to land at Oxnard Airport, Oxnard, California. During the subsequent forced landing, the airplane sustained substantial damage when it collided with a fence and building. The private pilot, who was the owner and builder of the airplane, received serious injuries. Visual meteorological conditions prevailed for the 14 Code of Federal Regulations Part 91 personal cross-country flight, and no flight plan was filed. The flight departed from Tehachapi, California, at an unknown time with an intended destination of Oxnard.

Oxnard Fire Department personnel reported that the airplane impacted the chain link fence backstop of a ball field and then struck a school bus barn. The wing separated from the fuselage and fuel was observed leaking from the wing.

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Accident occurred Tuesday, March 11, 2008 in Oxnard, CA
Probable Cause Approval Date: 4/30/2008
Aircraft: Bell 206B, registration: N7028J
Injuries: 1 Uninjured.
The pilot stated that he was performing an aerial application on a celery crop with the skids about 24-inches above the tops of the crop. While in straight and level flight, the landing skids contacted the crop and the helicopter pitched forward. The front of the skids dug into terrain and the helicopter tumbled before it came to rest on its side. Examination of the helicopter revealed substantial damage to the fuselage and the tail boom was separated. No mechanical anomalies were noted with the engine or flight control system.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:

The pilot's failure to maintain clearance with terrain during an aerial application.

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Accident occurred Friday, May 26, 2006 in Oxnard, CA
Probable Cause Approval Date: 7/25/2007
Aircraft: Piper PA-28-151, registration: N4596X
Injuries: 1 Serious, 2 Minor.
The aircraft collided with a car during a forced landing attempt following a loss of engine power in the traffic pattern. According to controllers in the Air Traffic Control Tower, the pilot reported that the engine quit shortly after takeoff from runway 25 as the airplane was on the upwind leg. The pilot was attempting to turn the airplane back for runway 7 when it touched down in a field and then struck a car traveling south on a city street, about a 1/4-mile west of the airport. A Federal Aviation Administration (FAA) airworthiness inspector responded to the accident site. He observed witness marks in an adjacent field that he indicated were tire marks from the landing gear of the airplane. The airplane then traveled in an easterly direction about 350 feet where it impacted and went through a chain link fence, crossed the north bound side of a city street, and collided with a sport utility vehicle (SUV) traveling southbound on the street. Responding
firefighters noted fuel leaking out of the left wing tank and found that the right wing tank was full of fuel. Subsequent interviews disclosed that multiple individuals manipulated the fuel selector valve in an attempt to staunch the flow of fuel, and the preimpact position of the fuel selector valve could not be reliably determined. The airframe and engine were subjected to detailed examinations and tests following recovery of the airplane to the airport. No evidence of a preimpact mechanical malfunction or failure was found that would explain the loss of engine power. The only anomaly was the fuel selector valve handle, which was of a non-standard size and configuration that would allow the valve handle to bypass the safety stop and rotate a full 360 degrees.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:

The loss of engine power for undetermined reasons.

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Accident occurred Friday, May 20, 2005 in Oxnard, CA
Probable Cause Approval Date: 9/13/2005
Aircraft: Piper PA-28-181, registration: N8460N
Injuries: 1 Uninjured.
The airplane's left wing impacted a building while the pilot was taxiing toward a transient parking area following an uneventful landing. When the pilot commenced a right turn and attempted to proceed between parked airplanes and a building, he diverted his attention toward the parked airplanes and misjudged his clearance from the building.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:

the pilot's failure to maintain an adequate clearance from the building. The pilot's diverted attention was a factor.

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Accident occurred Monday, March 07, 2005 in Oxnard, CA
Probable Cause Approval Date: 9/14/2007
Aircraft: Cessna 210L, registration: N2044S
Injuries: 5 Uninjured.
As the pilot turned the airplane onto the active runway, he saw white flashes coming from the engine gauges in the instrument panel. He did not believe there was a problem, and continued the takeoff run. About 1,000 feet down the runway, smoke started to enter the cabin, and he stopped the airplane and evacuated the passengers. When he returned to the cabin area, he noted a fire concentrated in the engine gauge instrument cluster area of the panel. He put the fire out, but by the time the fire department arrived, the fire had restarted. The cabin area sustained structural damage during the fire. Investigation found that the wire bundles in the engine gauge area had missing insulation and beading. The engine instrument section was removed for inspection, and a pinhole was found on the steel fuel pressure line. A Safety Board materials specialist examined the fuel pressure line, and noted copper material and damage that was consistent with electrical
arcing of a copper wire on another metal surface. The airframe manufacturer issued Service Bulletin SEB98-7 in 1998, which required an inspection of the fuel line between the firewall and fuel flow gauge for abrasion damage. No evidence was found that the service bulletin had been complied with. While the service bulletin was not mandatory, had it been addressed, the damage to the fuel line may have been found in a timely manner before the onset of the fire.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:

A pinhole leak in the fuel pressure line during the takeoff roll that was ignited by an electrical arc associated with wires adjacent to the fuel line. A contributing factor in the accident was the failure of maintenance personnel to comply with a manufacturer's service bulletin that addressed potential damage to the fuel line.

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Accident occurred Tuesday, November 09, 2004 in Oxnard, CA
Probable Cause Approval Date: 2/28/2006
Aircraft: American Eurocopter AS350-BA, registration: N655TV
Injuries: 2 Minor.
During a practice autorotation, the collective down lock engaged, which resulted in an uncontrolled descent and collision with terrain. The pilot and an instructor pilot were conducting the first practice autorotation of a planned series, and the pilot entered the autorotation about 500 feet above ground level. After lowering the collective the pilot kept the collective in the down position until he was in the flare. When the pilot tried to pull up on the collective, it would not move and both pilots saw that the collective down lock had engaged. Both pilots attempted to unlatch the collective, but they were unsuccessful. With the collective locked at flat pitch, the helicopter impacted the ground hard in a level attitude with some forward speed and it rolled over. Post accident investigation revealed the helicopter was equipped with an aftermarket avionics control panel. The collective lever lock is installed on this control panel console; it is a
spring steel plate with a hole in it to capture the collective locking tab. The lock also has a rubber grommet below the locking hole to dampen any vibration. With the collective in the full down position, the aftermarket console has about a 1/16-inch clearance between the lock plate and the collective lock tab, while the Eurocopter stock console panel has a 1/2-inch clearance. Exemplar aircraft with both the stock and aftermarket consoles were examined. In some of the aircraft, the grommet was not touching the console. This condition would allow the locking lever to vibrate and also decrease the clearance between the locking plate and the locking tab. This accident is the second known accident where the collective lock has inadvertently engaged in-flight with this particular aftermarket avionics panel installed.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:

The inadvertent in-flight engagement of the collective down lock, which resulted in an uncontrolled descent and ground impact. The collective down lock engagement was likely due to a combination of the reduced clearance between the lock plate and the collective with this avionics panel design, the collective down lock alignment/adjustment, and the tendency of the flexible lock plate to vibrate with the natural harmonic rhythmus of the helicopter.

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Accident occurred Saturday, December 27, 2003 in Oxnard, CA
Probable Cause Approval Date: 3/30/2005
Aircraft: Bellanca 7ECA, registration: N53879
Injuries: 1 Uninjured.
The airplane ground looped during the landing roll. After touchdown, the pilot applied right rudder and the pedal became stuck in a near full forward position. The pilot was then unable to maintain directional control and the airplane turned approximately 270 degrees on the runway and came to rest. A post accident inspection revealed that the pin that secured the right rudder pedal to the brake cylinder arm was missing. There was also evidence of aluminum shavings at the pin attachment point. An identical problem was discovered by the operator on the sister ship to the accident airplane. The pin on the sister ship was changed a few weeks before the accident. The operator intended to examine the rudder pedal pins on the accident airplane in the next scheduled maintenance period. The manufacturer of the airplane indicated that the pin can be installed either outboard or inboard of the cotter key. As depicted in Figure 26 of the Parts Manual, the
installation of the pin is depicted as inboard of the cotter key. In this model of the airplane, the battery is located in the forward section of the fuselage and a structural angle brace is installed for support. On the right pedal of the forward seat, the clearance between the pin and the angle brace is reduced with the angle brace in the design location if the pin is installed inboard of the cotter key. If the pin is installed outboard of the cotter key, it allows for greater clearance between the pin and the angle brace.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:

the failure of the pin that secured the right rudder pedal to the brake cylinder arm due to improper installation of the pin. Also causal was the manufacturer's confusing maintenance instructions regarding the installation of the right rudder pedal pin and cotter key.

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Accident occurred Sunday, September 08, 2002 in OXNARD, CA
Probable Cause Approval Date: 9/29/2004
Aircraft: Lockamy SONEX, registration: N164JL
Injuries: 1 Serious.
The experimental airplane experienced a propeller drive shaft failure and collided with the terrain during a forced landing at an airport. During the initial climb, about 300 to 400 feet above ground level, the engine surged and the airplane could not sustain lift. The engine was still producing power, but failed to distribute that power to the propeller. With a lemon grove directly ahead, the pilot opted to turn back to the runway to land. As he began a left turn toward the runway, the left wing impacted the dirt and the airplane "cartwheeled." Examinations revealed that the propeller hub had separated from the crankshaft. The tapered spacer, attached to crankshaft, had loosened. This instantaneous torque load to the crankshaft resulted in the propeller hub separating from the remaining taper, and the bolt unscrewing from the crankshaft.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:

the loosening of the tapered spacer, which resulted in the propeller hub separating from the crankshaft. A factor in the accident was the unsuitable terrain for landing.

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Accident occurred Sunday, April 22, 2001 in OXNARD, CA
Probable Cause Approval Date: 11/28/2001
Aircraft: Piper PA-22-135, registration: N75343
Injuries: 2 Uninjured.
The airplane made an off field forced landing following a loss of engine power during climb out from a touch-and-go landing. The pilot had practiced touch-and-go landings for over an hour and experienced no difficulties with the airplane. After a break, he completed another preflight inspection and practiced more landings. As the airplane climbed through 200 feet on the fourth takeoff, the engine made a clunking noise and stopped producing power. He steered the airplane to an open field and landed on soft dirt, but the airplane dug in and damaged the wings, stabilizer, landing gear, and propeller. The engine had accumulated about 1,860 hours since it had been manufactured in 1953, and the factory had no record of it returning since that time. The engine had accumulated about 910 hours since a field overhaul in 1960, and about 255 hours since a "top overhaul" in 1970, when the exhaust valves were replaced. All cylinders were undamaged except cylinder No.
3, which exhibited extensive mechanical damage. The exhaust valve for cylinder No. 3 fractured and separated where the valve stem transitions to the valve head. The fracture surfaces on the valve pieces were obliterated by the mechanical damage. The piston face exhibited mechanical damage over most of its surface, which contained two holes. The corresponding push rod was slightly bent, but there was no evidence of the valve sticking.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:

The fracture and separation of the number 3 cylinder exhaust valve head resulting in a loss of engine power and a forced landing. A factor in the accident was the soft field where the forced landing occurred.

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Accident occurred Thursday, November 16, 2000 in Oxnard, CA
Probable Cause Approval Date: 12/6/2002
Aircraft: Cessna 210K, registration: N8118G
Injuries: 2 Uninjured.
During the initial approach descent from cruise altitude, the engine lost power. The pilot richened the fuel mixture, which increased the engine vibrations. The pilot noticed the manifold pressure dropping and reduced the throttle. As power was reapplied, vibrations of a higher magnitude occurred. Los Angeles ARTCC (air route traffic control center) was notified of the emergency and directed the pilot to the nearest airport for landing. After considering the distance to the closest airport, the pilot decided to put the airplane down in a vacant dirt lot. The engine was installed the previous May and the postcrash inspection revealed a broken cam gear. The new engine was a factory remanufactured Continental IO-550. It replaced the original Continental IO-520, and its installation was authorized under a supplemental type certificate (STC).

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:

Failure of the internal cam gear in the remanufactured engine. A factor was the congested obstacles in the forced landing area.


Oxnard Airport Approach / Landing:

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