The mission of the "Redding Army Airfield" as it was then called was
advanced flight training for new airmen prior to deployment. In 1944 the
mission was changed from a training facility to a refueling and maintenance
base for transient aircraft.
After the war the airfield was turned over to the City of Redding to
operate as a civil airfield and military ownership ceased as of 1949.
Air Shasta Rotor and Wings; Bert Blanton School
of Flight; C and L Aero; Jim and I Aviators, Inc.; Redding Aerotronics,
Inc.; Redding Jet Center; Fuel; Air BP Jet-premix; 100LL; Helipads;
Restaurant on the field; Airport Deli; Peter Chu's Skyroom; Lodging within 4
miles;
Shasta Lake; Convention Center; Visitors Bureau;
Airport
Area Accident History:The builder/pilot reported that during the flight
he lost fuel pressure. He activated the second electric fuel pump, which
corrected the problem, but only for a few seconds. The engine lost then all
power. The pilot attempted to land in a dirt field. During the landing roll
the airplane nosed over.
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The pilot reported that while practicing night landings he misjudged the
timing of the touchdown flare, resulting in the airplane touching down hard
in a nose low attitude. Both lower engine mounts were broken and the top of
the aft fuselage was buckled. The pilot reported that no anomalies existed
with the airplane prior to the flight.
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The fight instructor reported that on the first landing the pilot-rated
student failed to extend the landing gear. The instructor further reported
that he didn't notice that the landing gear was in the UP position on
approach to landing. Additionally, the pilot-rated student had set the
manifold pressure at 15 inches, while the landing gear warning horn is set
to activate at 13 inches of manifold pressure. The flight instructor also
stated that the landing checklist was not accomplished. The airplane landed
with all three landing gear in the retracted position, which resulted in
substantial damage.
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The pilot stated that, while maneuvering on downwind within the airport
traffic pattern, he thought the fuel selector valve was on the "left" tank
and rotated the handle 1/4 turn in the clockwise direction to a position he
thought was "both." As the pilot turned onto base leg, he noticed the engine
had lost power and initiated a forced landing to an area adjacent to the
runway. Subsequently, the airplane landed hard on a rising embankment near
the runway and came to rest upright. The fuselage and both wings were
substantially damaged. The pilot reported that the fuel selector valve was
actually in the "right" position, and when he rotated the fuel selector
handle he had inadvertently positioned the valve to the "off" position. The
pilot added that there were no mechanical anomalies with the engine or
airframe prior to the accident.
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According to the pilot, during the landing on the 2,420-foot long runway, he
touched down about half way down the runway. He applied "heavy braking," but
felt the wheels skidding and eased off on the brakes. He decided not to go
around as he was "too far down the runway" when he realized he would not be
able to stop before overrunning the runway. The airplane exited the end of
the runway, traveled down an embankment and impacted a fence.
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The personal cross-country flight departed from Arlington, Washington, and
briefly stopped in Grants Pass, Oregon, departing about 1100 for a final
destination of Redding. While on a 2.5-mile final approach to the
destination airport, the engine experienced a loss of engine power and the
pilot performed an emergency landing in a field. The airplane collided with
a berm during the landing roll. Just prior to the loss of power, the right
fuel tank was empty and the left fuel tank had about 6 gallons of fuel
remaining; the fuel selector was positioned on the "both" selection.
According to the airplane's Owner's Manual, 5 gallons of fuel is unusable
per tank in non-level flight. The pilot did not refuel while en route.
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The airplane's left wing collided with a tree during a forced landing
following a loss of engine power. While on the approach for landing, the
engine lost power and the pilot attempted to land the airplane on a
residential street. The left wing collided with a tree during the landing
ground roll. Recovery personnel noted that no fuel was in the airplane's
fuel tanks, and fresh blue staining was evident on the belly area below and
behind the fuel strainer drain outlet. The pilot reported that the
airplane's fuel tanks had been filled the day preceding the flight, but he
could not provide fuel receipts. The airplane's performance specifications
state that at 3,000 feet, with 75 percent power and best power mixture, the
airplane cruises at 73 miles per hour and achieves a fuel consumption of 4.4
gallons per hour. The fuel capacity is 12 gallons. The straight line
distance between the departure and destination airports was 146 nm. The
airplane landed 4,500
feet short of the airport.
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The helicopter touched down hard at the culmination of a practice
autorotation. During the instructional flight lesson, the certified flight
instructor (CFI) monitored his student's flying. The student had about 15
hours of total helicopter flying experience. The CFI reported that the
student initiated the landing flare about 40 feet above ground level (agl).
According to the CFI, when the helicopter was about 10 feet agl he took over
the controls, raised the collective, and rolled on the throttle to initiate
a power recovery. The helicopter's low rotor warning horn sounded and the
respective annunciator light illuminated. Thereafter, the helicopter
contacted the ground, bounced, and came to rest after making two complete
rotations about its vertical axis. The tailboom and vertical stabilizer were
bent during the ground impact sequence. No mechanical malfunction or failure
was reported to have occurred.
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During cruise the airplane lost engine power and the pilot ditched the
airplane in a lake. The pilot said that during the preflight, he used a fuel
stick to determine the fuel quantity in each fuel tank. He indicated that
there was between 53 and 55 gallons of fuel onboard at the time of
departure. One hour into the flight, he switched fuel tanks from the left to
the right fuel tank, and planned to switch back to the left fuel tank after
another hour had passed. Once he arrived in the airport environment he
overheard a radio transmission from a departing aircraft, so he diverted
towards a nearby dam to allow the other aircraft time to depart the airport
environment. While in the vicinity of the dam at 1,200 feet above the ground
the engine quit. He immediately switched fuel tanks, turned on the fuel
boost pump, and advanced the throttle; however, the engine did not respond.
As he approached the dam, he observed power lines surrounding the dam. His
intention was to ditch the airplane in the water due to unsuitable terrain
in the area for an emergency landing. After the airplane cleared the power
lines, he made a descent towards the water. The airplane impacted the water
at 60 miles per hour. An engine inspection and teardown were conducted after
the aircraft was recovered from the lake with no discrepancies noted that
would have precluded normal operation. Eight gallons of fuel was recovered
from the left fuel tank, and no fuel was recovered from the right fuel tank.
No fuel was found in the fuel injector nozzles, that were found to be clear
of debris. The fuel lines were clear and intact. No fuel was found in the
engine driven fuel pump.
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The pusher configuration propeller departed the airplane during flight and
the airplane impacted trees during a forced landing in a field. The pilot
was established in cruise flight at 7,500 feet mean sea level when he felt a
vibration. The vibration then became "severe" and he heard a series of
clinking noises. He immediately began preparations for an emergency landing
because he knew that his propeller had separated from the airplane. The
pilot force-landed the airplane in a vacant field. The pilot stated that
about 2 weeks prior to the accident he had removed the wooden American
Propeller and installed a different propeller. The new propeller was too
long for ground clearance so the pilot reinstalled the original wooden
American Propeller. The original hardware was used to install the propeller
and the bolts were torqued to the recommended amount. The bolts were also
safety wired. After its installation, the propeller was operationally
tested. Prior
to its removal, the propeller had been installed on the airplane for about 1
year with no operational or mechanical problems noted. The pilot did not
have any other reported vibrations on flights leading up to the accident.
Post accident examination by the responding airport personnel showed that
the propeller and the attachment bolts were not on the propeller flange.
Three of the bolt holes showed evidence of rubbing and partial elongation of
the holes. The propeller and its attachment hardware were not recovered.
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The airplane's canopy separated from the cockpit during the landing descent,
and substantially damaged the empennage. The pilot indicated that he had not
experienced any malfunction with the canopy's operation when he initiated
the flight, and that the latch was in the closed position when the
separation occurred. A subsequent search for the separated canopy was
unsuccessful. An examination of the airplane revealed that the leading edge
of the left horizontal stabilizer was crushed inward over approximately a
1-foot-long span. Also, the leading edge of the vertical stabilizer was
similarly crushed in an aft direction. This was the first flight following
the company's removal and reinstallation of a serviceable canopy. The
company mechanics suggested that they may not have verified that the
canopy's locking pins were positively engaged in the support lugs on the
airframe during reinstallation of the canopy.