Rialto Municipal/Miro Field Airport, Rialto, CA
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Airport Area Accident History:
Accident occurred Sunday, October 26, 2008
in Rialto, CA
Aircraft: NAVAL AIRCRAFT FACTORY N3N-3,
registration: N44848
Injuries: 1 Uninjured.
This is preliminary information, subject to
change, and may contain errors. Any errors
in this report will be corrected when the
final report has been completed.
On October 26, 2008 about 1230 Pacific
daylight time, a Naval Aircraft Factory
N3N-3, N44848, experienced a loss of engine
power seconds after takeoff from runway 24
at the Rialto Municipal Airport, Rialto,
California. The airplane collided with
vegetation during the forced landing in an
open field about 1/2-mile southwest of the
airport. The airplane's lower right wing was
bent, and the airplane was substantially
damaged. The commercial certificated pilot
was not injured. Visual meteorological
conditions prevailed, and no flight plan was
filed. The personal flight was operated by
the pilot and performed under the provisions
of 14 Code of Federal Regulations Part 91.
The pilot reported to the National
Transportation Safety Board investigator
that the planned round-robin flight
originated about 1205 from the Flabob
Airport in Riverside. The pilot flew to
Rialto and landed without incident. The
accident occurred during the pilot's
attempted return flight to Flabob. The pilot
did not experience any problems with the
airplane prior to the mishap. The pilot
further reported that, as the airplane was
taking off, the engine's power began
surging. Then, upon reaching about 150 feet
above ground level, the engine lost all
power and the pilot elected to make a forced
landing in an open field ahead of the
airplane.
The pilot stated that when the engine lost
power, the event was not accompanied by any
unusual vibration, noise, or other anomaly.
= = =
Accident occurred Sunday, January 16, 2005
in Rialto, CA
Probable Cause Approval Date: 4/28/2005
Aircraft: Robinson R22B, registration:
N1122R
Injuries: 2 Uninjured.
During a practice full-touchdown
autorotation, the main rotor blades struck
and severed the tail boom. The certified
flight instructor (CFI) said that the
purpose of the flight was to prepare the
commercial pilot (student) for his CFI check
ride and they were performing full touchdown
autorotations. The helicopter was aligned
with the centerline of the south taxiway. At
60 feet agl, the student flared the
helicopter and then leveled it for a full
touchdown autorotation. When the helicopter
was 1 foot agl, the student pushed the
cyclic forward and the forward tips of the
skids touched the ground. The helicopter
rotated aft, and the CFI assumed the
controls and leveled the helicopter. Upon
touchdown, the main rotor blades contacted
the tail boom. The CFI noted no mechanical
malfunctions with the helicopter.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
the student pilot's improper use of the
cyclic control during a practice
autorotation, and the inadequate supervision
by the certified flight instructor
= = =
Accident occurred Monday, November 22, 2004
in Rialto, CA
Probable Cause Approval Date: 3/28/2006
Aircraft: Schweizer 269C, registration:
N45012
Injuries: 2 Uninjured.
The helicopter collided with terrain during
a pinnacle departure attempt. After
departing, the pilot configured the
helicopter into a hover about 3 feet above
ground level (agl) and verified that the
cockpit gauges were all displaying the
appropriate indications. In an attempt to
depart the area, he said he "began to trade
altitude for airspeed" while maneuvering in
a right turn, toward his planned escape
route consisting of downsloping terrain.
While in the turn, the rotor rpm became low
and he manipulated the throttle control for
full power, simultaneously lowering the
collective. Despite his attempts, the rotor
rpm failed to increase and the helicopter
continued to descend. In an effort to
cushion the impact, he raised the collective
just before the skids contacted terrain. The
helicopter rolled downhill, coming to rest
on its left side. The engine manufacturer
performed an engine test run; there were no
discrepancies or anomalies that would
indicate
the engine was not capable of running and
producing power prior to the mishap.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
the pilot's failure to maintain adequate
rotor rpm and altitude/clearance during the
takeoff initial climb.
= = =
Accident occurred Monday, December 29, 2003
in Rialto, CA
Probable Cause Approval Date: 3/30/2005
Aircraft: Cessna 210, registration: N6539X
Injuries: 2 Minor.
The airplane collided with ground obstacles
following a loss of engine power during a
VFR go-around. During a 200-mile instrument
cross-country flight, the pilot attempted to
lean the mixture while climbing to an
altitude of 10,000 feet; however, the engine
would sputter and cough. The pilot chose to
position the mixture in the "FULL RICH"
position. Unable to climb to the appropriate
altitude, the pilot canceled his IFR flight
plan and continued VFR with flight
following. About halfway through the flight,
the right wing fuel gage was indicating
empty, and though concerned about the
apparent abnormal fuel consumption, the
pilot decided to continue to his original
destination. The fuel selector was then
switched to the left fuel tank. At this
time, the airplane was flying over several
airports with maintenance and fueling
facilities. Approaching the destination, the
left fuel tank gage was indicating a low
quantity and the pilot declared an
emergency. The
pilot attempted to land at a nearby airport
but the airplane was too high and fast for
landing. The engine lost power during a
go-around attempt. Post accident examination
did not reveal any fuel staining on the
airplane. The vent lines and ports were
unobstructed and the fuel tank filler cap
seals were in good condition. Approximately
3 gallons of fuel were drained from the left
tank; approximately 10.5 gallons were
drained from the right fuel tank. According
to the POH for the airplane, the total fuel
system capacity is 65 gallons, with 5
gallons (2.5 for each tank) unusable. The
fuel selector has three positions, OFF,
LEFT, and RIGHT. The fuel selector was in
the "LEFT" position at the accident site.
Impact damage precluded functional testing
of the engine and the fuel metering unit.
Fueling records established that the
airplane was filled to capacity before
flight.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The pilot's inadequate in-flight
planning/decision by his fuel mismanagement
and his delay in initiating remedial action
which resulted in fuel exhaustion and the
loss of engine power.
= = =
Accident occurred Thursday, October 03, 2002
in Rialto, CA
Probable Cause Approval Date: 9/13/2005
Aircraft: McDonnell Douglas 600N,
registration: N625SB
Injuries: 2 Serious.
The sheriffs department helicopter was just
beginning an evening patrol flight when the
engine experienced a deceleration event
during transition from climb out to cruise
and the helicopter crashed into a
residential street during an attempted
autorotation. First responders to the
accident site, which included sheriff's air
unit mechanics, found the engine running at
idle and a fire in the engine compartment.
The helicopter had just come out of a
scheduled 100/300-hour inspection and this
was the first mission flight since the
maintenance. During the inspection, the
engine's fuel control Hydromechanical Unit
(HMU) had been removed for compliance with a
service bulletin. Prior to this flight, the
helicopter had completed a 10-minute post
maintenance flight check. The pilot in
command (PIC) conducted the preflight
inspection. The mission observer flight
officer, who held a private pilot
certificate with helicopter rating and was
attempting to upgrade to a
pilot position, had been given permission to
fly the helicopter and installed the dual
flight controls to the right side. No
problems were noted during the preflight,
and the takeoff was normal. About 500 feet
above ground level during the transition
from climb out to cruise, the pilot flying
heard the LOW ROTOR voice warning (two
times) followed by ENGINE OUT voice warning
(two times). Without initiating an
autorotation, he requested that the PIC take
the flight controls. Simultaneously, the PIC
had sensed a problem and took the flight
controls. Prior to and during the departure
up until the engine deceleration, the PIC
performed the observer flight officer
duties, which included radio communications
with dispatch, and had not monitored the
flight instrument readings or the progress
of the departure. The LOW ROTOR voice
warning activates when Nr falls below 95
percent. The voice warning system for ENGINE
OUT activates when N1 falls below 55 percent
or
a high rate of decay in N1. No discrepancies
were noted during the inspection of the
airframe. A teardown of the engine disclosed
no internal discrepancies; however, the fuel
inlet line fitting to the engine HMU was
found loose by two flats of the nut.
Functional testing of the fire damage ECU
(electronic control unit) found no
discrepancies. The HMU was installed in a
test bench and passed a functional check.
The fuel line inlet fitting nut was then
loosened incrementally one flat at a time
with a functional test conducted each time.
Significant fluctuations in metered fuel
output flow were noted during one test with
the nut three flats loose, and again at one
complete turn loose. These results could not
be reliably duplicated in subsequent tests.
The investigation found that the operator
had not established guidance for crew
resource management pertaining to crew
responsibilities, instrument monitoring
responsibilities, emergency procedures
initiation, or flight control transfer
procedures when flying in a dual pilot
operation.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
an engine deceleration event due to a loose
HMU fuel line fitting, which was a result of
inadequate maintenance procedures in the
100/300-hour inspection. Also causal was the
flying pilot's and pilot-in-command's
delayed recognition of the power loss, as
well as, the flying pilot's failure to
initiate an autorotation in a timely manner.
The pilot-in-command's failure to regain and
maintain adequate main rotor rpm was also
causal. A contributing factor to the
accident was the pilot-in-command's
inadequate supervision and diverted
attention due to his concentration on the
flight officer observer duties.
= = =
Accident occurred Sunday, April 01, 2001 in
Rialto, CA
Probable Cause Approval Date: 4/29/2003
Aircraft: Cessna 172N, registration: N739WE
Injuries: 2 Fatal.
A flight school Cessna 172N was destroyed
during a departure collision with
communication wires and terrain at Rialto,
California, about 0023 hours. The accident
flight was returning to Hawthorne,
California. The pilot had obtained a
standard weather briefing at 2319, for the
return flight. The pilot was advised of
airmets for IFR ceiling and visibilities for
his route of flight. The airplane had been
the subject of an Federal Aviation
Administration ALNOT, issued at 2210, for
failure to cancel an instrument flight plan
with Southern California Tracon from
Hawthorne to Rialto, an uncontrolled
airport. The pilot had obtained an FAA
preflight weather briefing at 1551, for the
flight to Rialto. According to the
instrument flight plan information, the
estimated time of arrival at Rialto had been
1845. Subsequently, the airplane was located
at the Rialto airport parking ramp by county
sheriff personnel. The ALNOT was canceled at
2240. The operator stated that
the pilot and passenger had flown to Rialto
to visit with friends and were to return to
Hawthorne. The pilot was a flight instructor
for the operator and was rated in airplane
single engine land and instrument. They
reported that he had accrued 650 total
flight hours. Radar data was obtained from
Southern California Tracon and a plot was
generated by a private vendor for Cessna
Aircraft Company. It shows the airplane
circling back over the airport and heading
northwest. The highest altitude before
coverage is lost is 1,700 feet mean sea
level.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The pilot's intentional visual flight into
instrument meteorological conditions.
Contributing to the accident was the pilot's
improper weather evaluation and lack of
total experience.
= = =
Accident occurred Monday, May 01, 2000 in
RIALTO, CA
Probable Cause Approval Date: 10/9/2001
Aircraft: Hughes 269C, registration: N5395S
Injuries: 2 Minor.
The helicopter landed hard and rolled over
during a practice autorotation. The CFI was
providing dual instruction to his student, a
CFI candidate. The student was handling all
of the controls, and he intended to perform
a 180-degree full touchdown autorotation.
During the maneuver, the CFI observed that
his student had allowed the airspeed to
decrease and the main rotor rpm to become
low. The CFI called the low rotor rpm
situation to his student's attention.
However, the student did not take decisive
corrective action by initiating a power
recovery in sufficient time to avoid the
resultant low rotor rpm flare and hard
touchdown. No mechanical malfunctions were
noted.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The student's misjudged altitude and failure
to maintain rotor rpm while practicing an
autorotation, and, the instructor's delayed
remedial corrective action and inadequate
supervision of the flight.
= = =
Accident occurred Friday, March 24, 2000 in
RIALTO, CA
Probable Cause Approval Date: 11/25/2003
Aircraft: Robinson R22 BETA, registration:
N8328Q
Injuries: 1 Fatal.
For undetermined reasons, the pilot began
hovering between 150 and 250 feet agl while
on final approach to the airport. He then
lost control of the helicopter and descended
in a nose low attitude until impacting the
ground. Earlier during the morning the pilot
had flown with his flight instructor (CFI)
on a round robin cross-country flight to the
same airport. According to the CFI, the
pilot had demonstrated that he was competent
to make the same flight solo, so the CFI
endorsed his logbook authorizing the flight.
Subsequently, the pilot departed on his
first solo cross-country flight in the
helicopter. Recorded radar data indicates
that the pilot proceeded to the destination
airport, entered its traffic pattern about
500 feet agl, and turned onto the base leg
while descending to about 200 feet agl. Two
witnesses observed the pilot on the final
approach leg. One witness reported that the
helicopter appeared to hover for 3 to 10
seconds, while the other
witness estimated it was stopped in the air
for 5 seconds. Both witnesses reported
seeing the helicopter's pitch attitude
decrease, then the helicopter descended
while in a 45-degree nose low attitude. The
on-scene accident site examination revealed
the helicopter impacted hard onto the level
ground while heading toward the airport. The
helicopter's landing gear structure
fragmented, and the main rotor blades bent
aftward. The helicopter came to rest 100
feet from the initial point of impact. No
evidence was found of any in-flight contact
between the main rotor blades and the
fuselage. No evidence was found of any
preimpact mechanical malfunction with the
flight control, driveline, and throttle
governor systems. The engine was test run
and full rated power was obtained. The pilot
was certificated to fly airplanes and had
about 110 hours of fixed wing flying
experience. His total dual and solo
experience flying the Robinson R22 was 29
and 5.7 hours,
respectively.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The pilot's in-flight loss of control for
undetermined reasons.
= = =
Accident occurred Friday, January 07, 2000
in RIALTO, CA
Probable Cause Approval Date: 7/10/2001
Aircraft: Cessna 177B, registration: N34021
Injuries: 1 Uninjured.
The accident flight was the first flight
following an oil change. While in cruise
flight about 38 minutes after takeoff, the
engine began to run roughly and the oil
pressure dropped to zero. The engine then
completely lost power and the pilot
attempted to land at the airport. He touched
down short of the runway and collided with a
fence. During the postaccident examination,
oil was evident on the firewall, rear engine
case area, and in the area of the oil
pressure screen housing, streaming aft on
the underside of the aircraft and on the
forward edge of both landing gear struts.
The screws that attach the oil pressure
screen were observed to be improperly
secured; there was no discernible torque
required to loosen the screws. The oil
pressure screen had been removed during the
oil change. The improperly torqued oil
screen housing bolts resulted in the loss of
oil, and the number 2 cylinder connecting
rod bearing failure and overheating of the
connecting
rod. The connecting rod released from the
crankshaft journal and punctured the upper
left crankcase, damaging the adjacent
components.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The failure of the maintenance personnel to
follow the manufacturer's procedures and
directives regarding the proper torquing of
the screws securing the oil pressure screen
housing, which resulted in the loss of
lubricating oil, and the subsequent seizure
of the engine.
Rialto Municipal/Miro Field
Airport Approach / Landing: