Rio Vista Municipal Airport, Rio Vista, CA
Airport History:
Rio Vista Airport
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Airport
Area Accident History:
Accident occurred Monday, July
18, 2005 in
Rio Vista, CA
Probable Cause Approval Date:
10/27/2005
Aircraft:
Cessna 152, registration:
N68475
Injuries: 1 Uninjured.
The student pilot bounced the
airplane during touchdown, lost
direction control, veered off
the runway, and nosed over.
During the approach, the pilot
realized that the crosswind was
very strong, which made control
difficult, and he decided to
execute a go around. On the
second approach attempt, he
decreased the airplane's
airspeed to approximately 60
knots, and still found the
crosswind to be very strong,
making the airplane difficult to
control. Shortly thereafter, the
airplane made contact with the
runway and bounced four times.
The student pilot lost
directional control of the
airplane and it veered off the
side of the runway onto the
grass median and nosed over.
During the preflight briefing
with his CFI, the instructor
told the student pilot to divert
to another airport if he could
not make the landing into
Rio Vista, California.
The pilot stated that the
airplane and engine had no
mechanical failures or
malfunctions during the flight.
The National Transportation
Safety Board determines
the probable cause(s) of this
accident as follows: the
student pilot's inadequate
recovery from a bounced landing
and his failure to maintain
directional control of the
airplane during landing rollout.
A contributing factor was the
student's failure to divert to
an airport with less severe
crosswind conditions.
===
Accident occurred Saturday,
August 28, 2004 in Rio Vista,
CA Probable Cause Approval
Date: 12/3/2004
Aircraft: Quicksilver MXL II,
registration: N4358Z
Injuries: 2 Uninjured. The light
experimental airplane was flying
northbound a few feet above an
unused levee dirt road and the
right wingtip struck a stand of
high bamboo growing along the
east side of the road. The
airplane then hit the road,
skidded off the road, and into
some large rocks along the
levee. Both occupants were
uninjured, and able to extract
themselves out of the wreckage.
The National Transportation
Safety Board determines the
probable cause(s) of this
accident as follows: the
pilot's failure to maintain
adequate clearance from high
vegetation while flying at a low
altitude.
===
Accident occurred Saturday,
February 02, 2002 in Rio Vista,
CA Probable Cause Approval Date:
9/30/2003
Aircraft: Robinette Ultra Pup,
registration: N2221X
Injuries: 2 Uninjured. The
experimental, amateur-built
airplane landed off-airport
following a total loss of engine
power on climb out. The pilot
reported that during the initial
climb after a slow-flight, low
pass down the 4,200-foot-long
runway and while about 200 feet
above ground level, the engine
lost all power although the
propeller continued to windmill.
After the accident, there was
about 9 gallons of 100-octane
aviation fuel aboard.
Earlier the same day he had
flown a prior flight leg on the
same tank of fuel. The pilot
suspected that carburetor icing
was the cause of the engine loss
of power. The airplane was
equipped with a
Mosler converted
automotive engine, and was
equipped with carburetor heat.
The carburetor heat control was
in the "on" position when engine
power was lost. A generic
carburetor icing probability
chart used by the Safety Board
showed the ambient temperature
and
dew point conditions to
have been within the region
marked "serious icing - cruise
or climb power." The National
Transportation Safety Board
determines the probable cause(s)
of this accident as follows:
The loss of engine power for
undetermined reasons.
===
Accident occurred Monday, March
13, 2000 in RIO VISTA, CA
Probable Cause Approval Date:
7/17/2001 Aircraft: Piper
PA-18-150, registration: N82751
Injuries: 1 Serious, 1 Minor.
The pilot had been maneuvering
low level in an area of wind
generators and power lines for
30 minutes. He started a slow
right climbing turn toward a new
work area, which was to the
right front of the airplane. The
sun was behind a cloud and he
could see power lines and wind
generators in the new work area.
Moments later the sun came from
behind the cloud and temporarily
blinded him. At that instant his
rear seat observer told him to
'look out.' He was flying up a
draw and noted wires angling
across his flight path. He
maneuvered to avoid them, but
contacted the last wire with his
right main gear. The airplane
fell to the ground when the wire
snapped. The National
Transportation Safety Board
determines the probable cause(s)
of this accident as follows:
failure of the pilot to maintain
clearance from power lines while
maneuvering at a low altitude. A
factor was glare from the sun.
===
Accident occurred Saturday,
January 22, 2000 in RIO VISTA,
CA Probable Cause Approval
Date: 7/15/2002
Aircraft: MINCE JURKA MJ77,
registration: N751JR
Injuries: 1 Uninjured. The pilot
made a forced landing in a
plowed field following a loss of
engine power. The airplane was a
3/4 scale P-51 replica with a
fuel injected automotive engine.
The flight departed Stockton
with full fuel onboard, which
was 32 gallons of fuel in two
16-gallon tanks, and the engine
burned about 14 gallons per
hour. While cruising at 3,500
feet, the airplane gradually
began to lose speed and
altitude. The manifold pressure
remained at a cruise setting,
but the pilot felt the engine
was not producing power. He
switched
fuel tanks from left to
right, cycled the ignition
switch, and adjusted the
mixture. The
engine coolant and oil
temperature gauges remained in
the green, but the power
continued to decline. The pilot
attempted to land in a plowed
field with the landing gear
down, but the landing gear
separated from the airplane and
damaged the wing spar. The pilot
reported that in order to assist
in the recovery, he drained all
of the fuel out of the left
fuel tank , and all but 5
gallons from the right tank the
day after the accident. The
recovery agent drained 5 gallons
of fuel from the
right fuel tank and no
fuel from the left tank. The
fuel selector valve had been
disconnected so he could not
tell what position it was in.
The fuel screen was clean and
clear of debris; the fuel
manifold distribution valve was
clean and contained no fuel. The
spark plugs were in good
condition. After several
attempts, investigators started
the engine and ran it up to
3,000 rpm. They were not able to
run it long because the water
pump belt was broken and they
couldn't get coolant to flow. A
shop owner in Stockton said the
airplane came in for an airshow
in October, but had engine
trouble. He rented the pilot
shop space to work on the
engine. He said the engine had a
broken valve and the pilot
repaired the engine himself. He
said he advised the pilot to fly
around the airport for an hour,
but the pilot said he had run
the engine on the ground for an
hour and experienced no
problems. The shop owner said he
observed the takeoff and thought
that the engine ran so rough
that it could not become
airborne. A company in Stockton
refueled this airplane and the
pilot's T-6 during the air show
with a combined total of 90
gallons and had no records of
refueling it since that time.
The National Transportation
Safety Board determines the
probable cause(s) of this
accident as follows: The loss
of engine power during cruise
flight for unknown reasons
resulting in a forced landing in
a plowed field.
Airport
Take-off/Approach / Landing: