Riverside Municipal Airport, Riverside, CA
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Airport Area Accident History:
Accident occurred Thursday, March 20, 2008 in
Riverside, CA
Probable Cause Approval Date: 4/30/2008
Aircraft: Ercoupe (Eng & Research Corp.) 415-D,
registration: N3942H
Injuries: 1 Uninjured.
The pilot fueled the airplane, sumped the wing
tanks, and departed. The engine lost power at the
end of the runway on climb out. He made a forced
landing on the grass infield of the airport. The
nose wheel went into a gopher hole, and the airplane
nosed forward. Post crash examination established
that the firewall sustained damage. The pilot
reported that he also found water in the gascolator,
and that the water most likely got into the fuel
system during recent rains. He opined that a more
thorough preflight could have prevented the
accident.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
Water contamination of the fuel system due to the
pilot's inadequate preflight and failure to
adequately drain the water from the fuel system.
= = =
Accident occurred Wednesday, February 27, 2008 in
Riverside, CA
Aircraft: Mooney M20C, registration: N591BB
Injuries: 3 Fatal.
This is preliminary information, subject to change,
and may contain errors. Any errors in this report
will be corrected when the final report has been
completed.
On February 27, 2008, at 2207 Pacific standard time
(PST), a Mooney M20C, N591BB, crashed during takeoff
from Riverside Municipal Airport (RAL), Riverside,
California. The Co-owner/Pilot was operating the
airplane under the provisions of 14 Code of Federal
Regulations (CFR) Part 91. The private pilot, and
two passengers were killed; the airplane was
destroyed by impact forces and the post crash fire.
The local personal flight departed at 2207, with a
planned destination of Corona Municipal Airport
(AJO), Corona, California. Visual night
meteorological conditions prevailed, and no flight
plan had been filed.
Interviews with the family and friends of the pilot
and passengers indicated that the flight departed
Corona for a local personal flight. The accident
airplane landed at Riverside Airport about 2000. The
pilot and passengers intended to eat at the airport
restaurant, but the restaurant was closed. The pilot
contacted his fiancée, who drove to the airport to
pick them up, and take them to a restaurant in the
local area for dinner.
After dinner they drove back to the airport, and the
pilot and passengers boarded the airplane for the
return flight to Corona. The fiancée did not wait at
the airport to see the airplane takeoff.
During takeoff a witness reported that once airborne
the airplane was "porpoising" up and down as it flew
towards him. As the airplane neared the end of the
runway, he saw it make a steep climbing left turn.
The witness stated that the airplane rolled inverted
and descended towards the ground in a nose down
attitude. The airplane then impacted a palm tree and
a vehicle that was parked on the residential street
located just south of the airport. After the
airplane impacted the ground, the witness saw an
explosion and a fire ball.
= = =
Accident occurred Tuesday, January 08, 2008 in
Riverside, CA
Probable Cause Approval Date: 2/28/2008
Aircraft: Robinson R-22, registration: N8280J
Injuries: 2 Uninjured.
The pilot reported that while making an approach to
a hover about 15 feet above ground level (agl), he
applied power and collective to stop the decent rate
and the helicopter began to yaw to the right.
Despite the pilot adding left anti-torque pedal and
increasing power, the helicopter continued to yaw to
the right and ascended 50 to 75 feet. The pilot
stated he lowered the collective and reduced power
until the helicopter descended through about 25 feet
agl, and then he raised the collective for landing.
Subsequently, the helicopter landed hard within
sandy terrain on the shoreline of a lake.
Examination of the helicopter revealed that the tail
boom and firewall sustained substantial damage. No
mechanical anomalies were noted during the
examination.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's misjudged landing flare and improper use
of the collective control.
= = =
Accident occurred Sunday, November 12, 2006 in
Riverside, CA
Probable Cause Approval Date: 12/20/2007
Aircraft: Ryan Navion B, registration: N5348K
Injuries: 2 Uninjured.
During the takeoff climb the engine lost power and
the pilot made a forced landing in an open field.
About 50-100 feet agl, with no remaining runway, the
engine began to run rough. Shortly thereafter the
engine lost all power. The pilot stated that he had
already raised the landing gear before the engine
began to run rough. He lowered the landing gear and
made the forced landing in the field. The landing
gear was only partially extended when the airplane
touched down. Post accident examination revealed
that air was leaking into the fuel system through
worn seals in the fuel selector valve and gascolator.
The Type Certificate Holder for the airplane issued
Service Bulletin (SB) 101A, which recommended
inspection of the fuel selector valve for leaks that
allow air intrusion. An annual inspection had taken
place 4 hours prior to the accident. Inspection of
the airframe logbooks revealed no record of SB 101A
having been performed.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
A leak in the fuel selector valve and gascolator
that resulted in fuel starvation on takeoff due to
air leakage into the fuel system. A contributing
factor in the accident was the inadequate annual
inspection performed by other maintenance personnel.
= = =
Accident occurred Tuesday, October 11, 2005 in
Riverside, CA
Probable Cause Approval Date: 1/31/2006
Aircraft: Bellanca 17-30A, registration: N14715
Injuries: 1 Uninjured.
The airplane impacted a fence following a loss of
control during landing. The pilot reported that he
had just made a normal landing when the airplane
veered off the runway to the left. The pilot
attempted to correct by applying right rudder
inputs, and when that had no effect, the pilot
attempted to execute a go-around by applying full
throttle, which only accelerated the left turn. The
airplane continued to the left until it impacted a
chain link fence located about 100 feet south of the
runway. Examination of the wreckage revealed the
nose wheel steering system consists of two rods
attached to the top of a T-bar supported by two
bearings mounted on the strut tube. The two rods,
one on the left and the other on the right, control
the steering of the nose wheel. The rod on the right
side was fractured and the surfaces exhibited
signatures consistent with tension overload failure.
The Federal Aviation Administration inspector who
responded to the scene
reported no skid marks were visible on the runway.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The failure of the steering control rod during an
unknown phase of the accident flight that resulted
in the unavailability of steering control upon
landing.
= = =
Accident occurred Saturday, May 01, 2004 in
Riverside, CA
Probable Cause Approval Date: 4/28/2005
Aircraft: Cessna 195, registration: N195AF
Injuries: 1 Uninjured.
The airplane veered off the runway and impacted a
ditch during the landing roll. The pilot had
completed 10 three-point practice touch-and-go
takeoff and landings without mishap, and was
attempting his last landing of the day. During the
landing roll, the airplane drifted off the
centerline to the right. The pilot attempted to
counteract the drift by applying left rudder
pressure. The airplane continued to veer in a right
arc off the side of the runway and encountered a
ditch. The airplane impacted terrain, pushing the
engine into the firewall and forcing the cockpit
floor upward. The pilot reported no mechanical
malfunctions with the airplane prior to impact.
Later, the pilot stated that the factors that he
thought contributed to the accident were a
quartering right tailwind, lack of left tail wheel
steering, impeded rudder control, pilot error/lack
of experience for not attempting to steer via the
use of differential braking, and the presence of a
ditch in close proximity to the runway. He reported
that there was a 4-knot right quartering tailwind
from 070 degrees. A Federal Aviation Administration
inspector examined the airplane and found no
evidence of a malfunction or failure with the brake,
control, or ground steering systems. The accident
flight was the pilot's first solo flight in the make
and model, although he had previously accumulated
about 140 hours in the same make and model.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's failure to maintain directional control,
resulting in a veer off the runway and collision
with terrain.
= = =
Accident occurred Saturday, February 14, 2004 in
Riverside, CA
Probable Cause Approval Date: 4/28/2004
Aircraft: Cessna 172S, registration: N262TA
Injuries: 1 Uninjured.
The airplane departed the taxiway and collided with
terrain while taxiing from landing. After taxiing
off the runway, the controller cleared the pilot to
taxi to the ramp area. He was unfamiliar with the
airport and requested further instructions. In an
effort to comply with what he thought the controller
was telling him to do, he departed the taxiway. He
continued down a grassy area and collided with a
median. The pilot reported no preimpact mechanical
malfunctions or failures with the airplane.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's inadequate visual lookout, which
resulted in his failure to maintain proper alignment
with the taxiway. Factors in the accident were the
dusk lighting conditions and pilot not understanding
the ground control taxi clearance.
= = =
Accident occurred Thursday, January 01, 2004 in
Riverside, CA
Probable Cause Approval Date: 6/8/2005
Aircraft: Piper PA-32R-300, registration: N589Q
Injuries: 4 Uninjured.
Following a catastrophic engine failure in cruise,
the airplane collided with multiple ground obstacles
during a forced landing in a field. The pilot
reported that while in cruise flight he first
noticed a "burning smell," which was followed a
short time later by a low oil pressure indication.
The pilot then felt a vibration, followed by a brief
engine overspeed to 3,000 rpm, and then the engine
lost all power. He performed a forced landing in a
field and collided with multiple ground obstacles.
Post accident examination of the engine at the
accident site revealed that the No. 6 connecting rod
had penetrated the engine crank case. An excess of
engine oil was found on the bottom of the airplane.
Further examination revealed an oil filter gasket,
Lycoming part number LW-13388, was extruded at the
base of the filter assembly and had allowed
virtually all engine oil to escape. A Lycoming
Mandatory Service Bulletin MSB-543, and an emergency
Airworthiness
Directive (AD) 2000-18-53, that was later superceded
by AD 2002-12-17, was applicable to this potential
problem, and required repetitive inspections and
gasket replacement or replacement of the gasket
adapter plate with a different part number. The
investigation could find no evidence of compliance
with either AD.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
engine oil exhaustion due to the extrusion of an oil
filter converter plate gasket and the failure of the
aircraft owner to comply with a mandatory Service
Bulletin and a Federal Aviation Administration
emergency Airworthiness Directive.
= = =
Accident occurred Sunday, August 24, 2003 in
Riverside, CA
Probable Cause Approval Date: 11/25/2003
Aircraft: Cessna 172M, registration: N64291
Injuries: 2 Uninjured.
The airplane collided with terrain during landing.
The pilots were practicing a short field landing
with the student pilot at the controls. The airplane
got low on short final. The CFI recognized that the
airplane was too low, took over the airplane
controls, and simultaneously added power and raised
the nose. The airplane struck a berm that led up to
the approach threshold of the runway. The airplane
bounced and came to rest on the approach end of
runway.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The student pilot's misjudged distance and altitude,
and the instructor's inadequate supervision of the
flight. Also causal was the instructor's delayed
remedial action.
= = =
Accident occurred Friday, June 13, 2003 in
Riverside, CA
Probable Cause Approval Date: 12/28/2004
Aircraft: Eurocopter France AS 350 B2, registration:
N6087C
Injuries: 2 Uninjured.
The public use operator of the helicopter reported
that the purpose of the flight was for the flying
pilot to receive an annual proficiency check. During
a simulated "stuck" anti-torque pedal emergency
landing procedure, the flying pilot attempted to
land the helicopter on a hard surfaced runway while
the helicopter still had significant yaw. The
helicopter touched down twice, and landed hard on
the second touchdown, resulting in structural damage
to the helicopter's fuselage and drive train
components. Both pilots held flight instructor and
airline transport certificates. The check pilot did
not intercede or apply remedial action while the
flying pilot was attempting to land with the
simulated stuck pedal.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The flying pilot's failure to align the helicopter
during a simulated emergency landing, which resulted
in a hard landing and structural damage to the
helicopter. A factor associated with the accident
was the check pilot's failure to initiate remedial
action.
= = =
Accident occurred Saturday, May 31, 2003 in
Riverside, CA
Probable Cause Approval Date: 12/28/2004
Aircraft: Winters Glasair SH-2, registration: N73VL
Injuries: 1 Fatal.
The experimental single-engine airplane collided
with terrain following a loss of control after
takeoff. Witnesses reported seeing the airplane
takeoff, climb to 200 to 300 feet (agl), make a
sharp left turn, and nose-dive into the ground. A
post-accident examination of the wreckage revealed
no evidence of pre-impact anomalies to the airframe
or engine.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's failure to maintain control of the
airplane during an abrupt, low altitude maneuver
during the takeoff-initial climb, which resulted in
a collision with terrain during the subsequent
uncontrolled descent.
= = =
Accident occurred Monday, October 21, 2002 in
Riverside, CA
Probable Cause Approval Date: 12/28/2004
Aircraft: Cessna 210C, registration: N9788X
Injuries: 1 Serious, 2 Minor.
During the instrument approach the engine quit, and
the pilot attempted a forced landing in hilly
terrain and poor visibility. According to flight
planning information recovered from inside the
airplane, it had departed with full fuel (63.5
useable gallons). The airplane had been airborne for
about 3:17 hours at the time of the accident. Prior
to disassembly of the airplane for recovery, the
recovery agent drained the fuel tanks. The left tank
had about 13 gallons of blue liquid with the odor of
aviation gasoline, and the right tank was empty. The
manufacturer ran the engine in a test cell. It
performed normally without any hesitation or
interruptions in power from idle to full throttle.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's failure to position the fuel selector to
the tank containing fuel resulting in a loss of
engine power due to fuel exhaustion.
= = =
Accident occurred Thursday, July 05, 2001 in
RIVERSIDE, CA
Probable Cause Approval Date: 12/30/2003
Aircraft: Bell 47D-1, registration: N64580
Injuries: 2 Uninjured.
The helicopter experienced a rough running engine on
short final approach and entered an autorotation,
but made a hard landing and sustained substantial
damage. The crankshaft failed as the result of
fatigue cracking initiated by surface damage and
localized overheating. The crankshaft was reportedly
overhauled 165 hours prior to the failure. Optical
examinations of the fracture faces found beach marks
and crack arrest lines indicative of fatigue
cracking though the majority of the crank cheek.
Further examinations established that the fatigue
initiated at two origins on the aft radius surface
of the No. 3 main bearing journal about halfway
between the journal and cheek surfaces. An oil stain
covered the aft radius and cleaning revealed wide
spread surface damage to the radius. The presence of
an oil stain on top of the damage indicates that the
damage occurred either during the overhaul or soon
there after and was not a result of the failure. The
damage
extended from the journal surface up to the level of
the origin area and completely around the journal.
The surface damage consisted of circumferential
scoring, intermittent tearing, and material flow.
The radius also had a slight bronze hue. Further
cleaning and inspections found similar damage and
coloration on the forward radius of the No. 3 main
bearing but no damage to other journal radii. The
direct visual examination of the No. 3 main bearing
journal surface showed heavy circumferential scoring
and roughening but no visual indications of
overheating. The majority of the other journals,
both rod and main, also displayed similar scoring
but to lesser degrees. Measurements established that
the diameters of all main bearing journals were
between 2.238 and 2.240 inches. All rod journals
measured 1.927 inches in diameter. Conversations
with a distributor for new Franklin engines
indicated that standard bearing sizes for 6A-335
engines are 2.250 to
2.249 inches for mains and 1.9375 to 1.9365 inches
for rods. Bearings for 0.010- and 0.020-inch
undersize journals are available for both the main
and rod journals. The measurements on the fractured
crankshaft are consistent with 0.010 inch under size
journals for both the mains and rods. The presence
of a white layer along with the undersized journals
does indicate that the crankshaft had been
renitrided at some point in time. The Franklin
6V-335 was originally certificated in 1956. The type
certificate is now held by iyPZL-RzeszowlÈ (PZL) of
Poland.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The engine crankshaft's failure as the result of
fatigue cracking initiated by surface damage and
localized overheating due to the installation at
overhaul of incorrectly sized bearings.
= = =
Accident occurred Tuesday, May 08, 2001 in
Riverside, CA
Probable Cause Approval Date: 7/15/2002
Aircraft: Beech BE77, registration: N3865D
Injuries: 1 Minor.
According to the student pilot, he was practicing
ground reference maneuvers over and around Lake
Mathews. He said he was finishing up a few power on
and power off stalls, when he thought he would
practice a couple of emergency landings. He said he
was familar with the procedure and had practiced
them several times with no problems. The first
attempt was sucessful. However, on the second
attempt, he began his climb-out, flaps fully
extended with full power. He was subjected to
turbulence from the right, raising the right wing,
at which time he lost some altitude. He regained
control with aileron and rudder input. He realized
that he was not climbing, instead he was losing
altitude. He said that he never regained enough
altitude to raise the flaps. He made a forced
landing in rough terrain and thick brush, collided
with a bush and nosed over.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The student pilot's failure to maintain appropriate
airspeed and to configure the airplane for
climb-out.
= = =
Accident occurred Saturday, May 05, 2001 in
Riverside, CA
Probable Cause Approval Date: 1/23/2002
Aircraft: Aero Commander 112A, registration: N1159J
Injuries: 1 Uninjured.
On the landing rollout, the airplane veered to the
right, departed the runway, and collided with a
ditch. The purpose of the flight was to conduct
three takeoffs and landings for currency. The
accident landing was the first landing of the day.
On the landing rollout the airplane went to the left
and the pilot corrected back to runway centerline.
The airplane then moved to the right of centerline.
The pilot attempted to correct back to runway
centerline with left rudder input and then left
brake; however, the airplane continued to the right
and into a ditch. A postaccident examination of the
nose wheel and steering assembly revealed excessive
play or wear that may have reduced steering control.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
Failure of the pilot to maintain directional control
of the airplane during the landing roll. A factor
was the worn nose wheel steering assembly.
= = =
Accident occurred Tuesday, April 11, 2000 in
RIVERSIDE, CA
Probable Cause Approval Date: 7/17/2001
Aircraft: TAYLOR SMITH WITMAN W-10, registration:
N90TS
Injuries: 1 Minor.
The pilot made a 3-point landing, then bounced back
into the air. He added power and the airplane veered
to the left. The airplane departed the runway and
collided with a fence running parallel to the
runway.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
failure of the pilot to recover from a bounced
landing resulting in a loss of directional control
and collision with a fence.
Riverside Muncipal
Airport Approach / Landing: