Brown Field Airport, San Diego, CA
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Brown Field Airport Today:
Airport
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Airport Area Accident History:
Misc San Diego Accidents:
Accident occurred Tuesday, June 24, 2008 in
San Diego, CA
Probable Cause Approval Date: 7/30/2008
Aircraft: Cessna 172M, registration: N9629V
Injuries: 1 Uninjured.
The student pilot reported that he was
practicing touch-and-go landings and made a
normal landing on runway 28L. Witnesses
located adjacent to the runway observed the
landing, and stated that the airplane landed
hard on the right main landing gear. During
the landing roll, the pilot raised the
flaps, turned the carburetor heat off, and
started to increase engine power when the
airplane then began to veer to the left. He
then applied full engine power in an attempt
to get the airplane airborne. The airplane
became airborne and the left main landing
gear struck a taxiway sign. The pilot then
elected to abort the takeoff and he reduced
engine power, switched off the master switch
and turned off the magnetos. The airplane
continued into the adjacent ramp area and
struck a parked and unoccupied helicopter.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The student pilot's failure to maintain
directional control during a touch-and-go
landing.
= = =
Accident occurred Sunday, August 12, 2007 in
San Diego, CA
Probable Cause Approval Date: 11/29/2007
Aircraft: Cessna 195, registration: N1031D
Injuries: 2 Uninjured.
According to the pilot, the landing approach
to runway 27R was normal. He asked the local
controller for the winds and was told they
were from 260 degrees at 7 knots with no
reported wind gusts. He flared the airplane
for a touchdown in "a three point landing
attitude." As expected, he heard the stall
warning horn go off, felt the tail wheel
begin to touch the runway and was expecting
the main gear wheels to touch when he "felt
the airplane quickly surge up and then slam
down." The pilot reported that "it felt like
a gust of wind lifted the airplane at the
last moment." The airplane "stalled" at an
altitude of 8 to 10 feet above the runway
and struck the ground "extremely hard."
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The pilot's inadequate compensation for a
wind gust that ballooned the airplane during
the landing flare, which resulted in a hard
landing. A contributing factor was the wind
gust.
= = =
Accident occurred Saturday, August 11, 2007
in San Diego, CA
Probable Cause Approval Date: 11/29/2007
Aircraft: Cirrus Design Corp. SR22,
registration: N336SR
Injuries: 3 Uninjured.
According to the pilot, his landing approach
was "a little low" so he added power to
compensate. Upon touchdown, the airplane
bounced "much higher" then he had previously
experienced. He increased airspeed in an
attempt to "make a more controlled landing."
The airplane touched down and bounced "even
higher." The airplane touched down a third
time, and the nose wheel collapsed.
Examination of photographs revealed
structural damage to the bottom of the
fuselage aft of the firewall.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The pilot's improper recovery from a bounced
landing, which resulted in porpoising and
collapse of the nose landing gear.
= = =
Accident occurred Friday, December 01, 2006
in San Diego, CA
Probable Cause Approval Date: 3/31/2008
Aircraft: Learjet 36, registration: N26FN
Injuries: 3 Uninjured.
The airplane sustained an in-flight loss of
the right elevator during an in-flight upset
while maneuvering. The pilot was flying the
airplane from the left seat. The mishap
airplane rendezvoused with another Learjet
to begin a series of profiles for flight
testing. The crew noted that the horizon was
very difficult to discern. While maneuvering
for the second set of data points, the pilot
lost sight of the other airplane, and rolled
right to remain clear. His vision was
impaired by the glare from the sun, which
delayed his recognition of the airplane
entering an unusual attitude. The pilot
initiated recovery with the airplane in an
estimated 70-degree right bank, 50-degree
nose down attitude, and an airspeed of 380
KIAS. During the dive, the crew noted that
the airplane was definitely shuddering, but
did not recall any rolling tendencies or
vibration of the control yoke. The crew
conducted a controllability check by slowing
it to 150 KIAS and lowering
the landing gear. Again the airplane
exhibited no unusual flight characteristics.
The remainder of the flight and landing were
uneventful. During post flight inspection,
the aircrew discovered that the right
elevator was missing.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The pilot's failure to maintain aircraft
control while maneuvering, which resulted in
exceeding the design stress limits of the
aircraft. Contributing to the accident was
the sunglare.
= = =
Accident occurred Friday, October 15, 2004
in San Diego, CA
Probable Cause Approval Date: 3/28/2006
Aircraft: DeRosier DR-107, registration:
N31SH
Injuries: 1 Fatal.
The airplane impacted terrain while the
pilot was performing low-level aerobatic
maneuvers at an airshow. Review of
videotaped footage of the pilot's
performance showed that about 15 minutes
into the flight, the pilot began a rolling
maneuver that the airplane was to pull out
of and continue parallel to the ground. The
airplane never pulled out of the downward
flight path and impacted terrain. This
particular airshow was a milestone for the
pilot and there may have been self-induced
pressure to perform well.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
the pilot's failure to maintain adequate
clearance from terrain while performing
low-level aerobatic maneuvers.
= = =
Accident occurred Thursday, January 22, 2004
in San Diego, CA
Probable Cause Approval Date: 4/28/2004
Aircraft: Beech B36TC, registration: N321JT
Injuries: 1 Uninjured.
The airplane overran the runway, and
collided with runway end identifier lighting
and a ditch during an attempted go-around.
The airplane landed long, and the pilot
applied brakes upon touchdown. The left main
tire blew out and the pilot attempted a
go-around. The airplane overran the runway
and veered to the left, resulting in the
left wing colliding with a runway end
identifier light. The airplane continued to
the left and encountered a ditch filled with
soft mud. The pilot did not report any
mechanical problems with the airplane prior
to the accident.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
the pilot's misjudged speed and altitude,
which led to a failure to attain the proper
touchdown point and a subsequent runway
overrun. Also causal was the pilot's delayed
decision to perform a go-around.
= = =
Accident occurred Thursday, December 04,
2003 in San Diego, CA
Probable Cause Approval Date: 12/28/2004
Aircraft: Cessna 525, registration: N15C
Injuries: 3 Uninjured.
The airplane veered off the runway during a
night landing in instrument conditions and
collided with ground obstructions. The
weather conditions included a visibility of
less than 1/4-mile in fog, with a vertical
visibility of 100 feet. The pilot stated he
was able to see the field while intercepting
the instrument approach course at 3,000 feet
msl. Using instruments for the approach, he
was still able to maintain visual contact
through the 100- to 200-foot-thick layer of
fog, when he reached 200 feet agl. After
descending, he lost visual contact with the
runway, and everything became black. He
started to move the levers up for a
go-around, but noticed two red lights to his
left. He thought he was too close to the
ground and too slow, so he decided to land.
The airplane touched down on the runway a
second or two later. The pilot did not
maintain directional control and the
airplane veered to the left. It crossed an
unpaved area, then hit and crossed a
taxiway. The pavement lip edge broke the
nose wheel off. The airplane continued onto
another unpaved area and came to rest. It
was about 50 feet to the left of runway 28R,
and about 100 feet to the right of runway 5.
The airplane also incurred damage to the
nose gear fork assembly, pressure vessel,
and to frame members. The pilot stated that
the accident could have been prevented had
he initiated a go-around when he lost visual
contact with the runway. He reported no
preimpact mechanical malfunctions or
failures with the airplane.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The pilot's failure to maintain directional
control and to initiate a timely go-around
when visual contact with the runway was
lost.
= = =
Accident occurred Sunday, October 26, 2003
in San Diego, CA
Probable Cause Approval Date: 2/24/2005
Aircraft: Mooney M20K, registration: N1147N
Injuries: 1 Uninjured.
The airplane landed hard on a highway while
attempting to perform a go-around from
runway 28R. The pilot received a preflight
weather briefing from 1120 to 1131 and was
advised he could not file IFR into the
destination airport due to the closure of
the TRACON and the airport ATCT due to a
major forest fire threatening the
facilities. He was advised he "might be able
to get in VFR." He filed IFR to an
intersection located in the vicinity of his
destination airport. Once the flight arrived
in the general destination area, the pilot
canceled his IFR clearance and flew visually
to the airport. After attempting to land
runway 28R, he applied power for a
go-around. He retracted the flaps but left
the landing gear down, and did not put the
propeller control in the full forward
position. As the pilot maneuvered during the
go-around he turned into a tailwind
situation and the airplane was unable to
maintain a climb. The airplane descended to
impact on a highway.
A post crash fire erupted and consumed the
airplane. The POH for the airplane states
that the propeller control should be at a
high rpm during landing. For a go-around
procedure, the POH indicates that the pilot
should apply power, retract the flaps to the
takeoff position [10 degrees], and then
retract the landing gear and remaining flaps
once the airplane accelerates to 91 mph (77
knots) IAS. A post-accident inspection
revealed that the propeller governor control
arm was 3/8-inch from the low pitch stop. A
METAR was issued at 1414 that noted the wind
was from 070 degrees at 6 knots, gusting to
14 knots. No discrepancies were found duirng
an examination of the engine.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
the pilot's failure to configure the
airplane properly for the go-around which
resulted in degraded climb performance, and
his failure to maintain adequate airspeed
which resulted in a stall. The tailwind was
a contributing factor.
= = =
Accident occurred Wednesday, April 26, 2000
in SAN DIEGO, CA
Probable Cause Approval Date: 5/18/2001
Aircraft: Robinson R22 BETA, registration:
N622EH
Injuries: 1 Fatal, 1 Serious.
According to the student pilot, he was a
rated commercial pilot working toward his 20
hours of indoctrination into the aircraft.
'We were going to practice emergency
procedures in the aircraft and get a little
bit more familiar with flying it.' The
student was flying the helicopter and
decided to fly over an Indian Reservation to
look at their motocross track for future
photography work in the helicopter. The
student told the instructor to take the
controls and fly a racetrack pattern over
the track and make an aerial application
type turn at the end of the track to reverse
course. The student would then try and
duplicate the maneuver. As they changed
controls from one another they would say,
'You got it,' or ' Okay, I got it' to
confirm the transition. After the maneuvers
were completed over the track, a critiquing
took place while the student was flying in a
hover. After the critiquing the student
reported that he told the instructor to fly
us out of
here and we will go over to Ramona.
According to the student, when the
instructor took the controls he said, 'I got
it.' About the same time, the student said
that the helicopter drifted a little bit and
lost a little altitude. The student got back
on the controls and the instructor said 'I
got it' and he let go. The helicopter again
drifted a little bit and the student saw
through the lower bubble a rock sticking up
out of the brush. The brush was about 5 feet
high. The helicopter drifted over, the skid
hit the rock, and the helicopter went into a
dynamic rollover. The Safety Board examined
the wreckage after recovery. There were no
airframe or engine pre-accident
discrepancies or mechanical malfunctions
observed during the examination of the
recovered remains.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The failure of the flight instructor to
maintain control of the helicopter,
resulting in skid contact with an obstacle
and dynamic roll over.
= = =
Accident occurred Saturday, March 11, 2000
in SAN DIEGO, CA
Probable Cause Approval Date: 6/25/2003
Aircraft: Robinson R22B, registration:
N7078B
Injuries: 2 Uninjured.
The pilot landed the helicopter in the
parking lot where his business was located
to drop off a passenger and complete some
business. After completing his business he
elected to takeoff in a northerly direction
along the west side of the building toward a
parked van. This placed him a position to
depart without a clear takeoff flight path,
effectively eliminating his ability to
remain in ground effect until entering
translational lift. The pilot lifted to a
hover, took off, and started his departure
to the north. About 50 feet along the
takeoff path, at an altitude of
approximately 16 feet agl, the pilot noted a
decrease in rotor rpm. He realized he would
not be able to complete his planned
departure and elected to execute a forced
landing into the parking lot. He set the
helicopter down in the parking lot as he
veered to the right to avoid hitting the
van. The tail rotor came into contact with
the office window, breaking the window, and
severely
damaging the tail rotor and the tail rotor
gearbox.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The pilot's selection of an inadequate
takeoff area which precluded his ability to
remain in ground effect until entering
translational lift and resulted in his
failure to maintain main rotor rpm.
Accident occurred Saturday, March
03, 2007 in San Diego, CA
Probable Cause Approval Date:
5/29/2007
Aircraft: Hirsch Thorp T-18,
registration: N78DH
Injuries: 2 Minor.
The conventional gear airplane
bounced two times after touchdown
and nosed over. On the first bounce,
the pilot added a small amount of
power to allow the airplane to
settle back onto the runway.
However, the airplane bounced again,
and he added full power in an
attempt to go around and pushed
forward on the control stick. The
propeller then contacted the runway
and the airplane nosed over. The
pilot stated that there were no
mechanical failures or malfunctions
during the flight.
The National Transportation Safety
Board determines the probable
cause(s) of this accident as
follows:
The pilot's improper bounced landing
recovery and improper use of the
flight controls that resulted in a
porpoise and a nose over.
= = =
Accident occurred Saturday, August
20, 2005 in San Diego, CA
Probable Cause Approval Date:
2/26/2007
Aircraft: Patch Dan F Varieze,
registration: N862DP
Injuries: 1 Fatal.
Witnesses observed the airplane on a
normal final approach and then it
made a sudden right turn and
impacted tractor trailers in a
storage yard about 0.4 miles from
the runway. The witnesses did not
hear any unusual noises emanating
from the engine. No evidence of
preimpact mechanical malfunction was
observed with the airframe systems.
During the disassembly of the
carburetor, investigators noted that
the accelerator pump seal was worn
and separated from the retainer
spring, which may have prevented the
engine from responding to the
pilot's throttle input.
The National Transportation Safety
Board determines the probable
cause(s) of this accident as
follows:
a divergence from the final approach
course and an in-flight collision
with storage containers for
undetermined reasons.
= = =
Accident occurred Sunday, April 23,
2006 in San Diego, CA
Probable Cause Approval Date:
1/31/2007
Aircraft: Grumman American AA-1C,
registration: N9756U
Injuries: 2 Minor.
The airplane stalled during the turn
onto the crosswind leg, and it
impacted the ground and a fence. The
pilot reported that no mechanical
malfunction was experienced during
the flight. Regarding the sequence
of events leading to the accident,
the pilot reported that he had
received permission from the local
air traffic controller to perform an
early turn onto the crosswind leg
following takeoff. According to the
pilot, during the climb the
passenger spoke, and he diverted his
attention toward the passenger. Upon
looking forward, the pilot noticed
that the airplane was stalling. The
airplane impacted the ground before
he was able to regain control.
The National Transportation Safety
Board determines the probable
cause(s) of this accident as
follows:
The pilot's failure to maintain
adequate airspeed, which resulted in
a stall during initial climb. A
contributing factor was his diverted
attention.
= = =
Accident occurred Sunday, October
24, 2004 in San Diego, CA
Probable Cause Approval Date:
5/26/2006
Aircraft: Learjet 35A, registration:
N30DK
Injuries: 5 Fatal.
The Safety Board adopted the final
report of this accident
investigation, including the
analysis and probable cause, on May
23, 2006. The Board's full report is
available on :
http://www.ntsb.gov/publictn/2006/AAB0605.pdf
On October 24, 2004, about 0025
Pacific daylight time, a Learjet 35A
twin-turbofan airplane, N30DK,
registered to and operated by Med
Flight Air Ambulance, Inc. (MFAA),
collided into mountainous terrain
shortly after takeoff from Brown
Field Municipal Airport (SDM), near
San Diego, California. The captain,
the copilot, and the three medical
crewmembers received fatal injuries,
and the airplane was destroyed. The
repositioning flight was operated
under the provisions of 14 Code of
Federal Regulations (CFR) Part 91
with an instrument flight rules
(IFR) flight plan filed. Night
visual meteorological conditions
prevailed. The flight, which was the
fourth and final leg of a trip that
originated the previous day,
departed SDM at 0023.
The National Transportation Safety
Board determines the probable
cause(s) of this accident as
follows:
The failure of the flight crew to
maintain terrain clearance during a
VFR departure, which resulted in
controlled flight into terrain, and
the air traffic controller's
issuance of a clearance that
transferred the responsibility for
terrain clearance from the flight
crew to the controller, failure to
provide terrain clearance
instructions to the flight crew, and
failure to advise the flight crew of
the MSAW alerts. Contributing to the
accident was the pilots' fatigue,
which likely contributed to their
degraded decision-making.
= = =
Accident occurred Saturday, March
08, 2003 in San Diego, CA
Probable Cause Approval Date:
9/1/2004
Aircraft: Kolb Company Firestar,
registration: N670JW
Injuries: 2 Uninjured.
The airplane nosed over following an
emergency landing in an open field.
The pilot was flying westward toward
the coastline at 1,500 feet. He
heard a "bang," and then felt
abnormal vibrations. He elected to
perform an emergency landing in an
open field. Upon landing in the soft
ground the airplane nosed over.
Initial inspection revealed a
splintered propeller. The
manufacturer's examination of the
carbon fiber composite propeller
revealed numerous indentations on
the leading edges and patterns
consistent with a foreign object
strike that occurred prior to blade
delamination. The manufacturer
identified a 1.9-inch-wide abrasion
mark along the entire blade width
that resembled patterns that are
commonly associated with nylon
safety belt webbing. The aircraft
kit manufacturer reported that the
standard harness webbing provided by
them is 1.75 inches wide. The pilot
said that the rear seat of the
airplane had the standard factory
supplied 3-point harness
webbing and the pilot seat had an
after market 4-point harness. The
airplane is a high wing design, with
the wing mounted above and behind
the open cockpit. The engine and
pusher propeller are mounted on top
of the wing.
The National Transportation Safety
Board determines the probable
cause(s) of this accident as
follows:
propeller delamination due to the
pilot's failure to properly secure
the rear seat shoulder harness prior
to flight. A contributing factor was
the soft ground in which the
airplane landed.
= = =
Accident occurred Saturday, May 11,
2002 in San Diego, CA
Probable Cause Approval Date:
3/2/2004
Aircraft: Cessna 170B, registration:
N3462C
Injuries: 2 Uninjured.
The airplane veered off of the
runway, ground looped, and impacted
a ditch. The flight instructor
reported that the student was flying
as they entered the traffic pattern
with the intention of performing
touch-and-go pattern operations.
Upon touchdown, the airplane veered
to the right. By the time the flight
instructor took the controls, the
airplane was headed off of the
runway. He added power in an attempt
to abort the landing; however, the
airplane veered off of the runway.
The instructor noted that he let the
student go too far before he
intervened. He reported that there
were no mechanical malfunctions or
failures. The winds at the time of
the accident were from 300 degrees
at 10 knots gusting to 15.
The National Transportation Safety
Board determines the probable
cause(s) of this accident as
follows:
The failure of the dual student to
maintain directional control of the
airplane and the instructor's
delayed the remedial action, which
resulted in a ground loop. A factor
in the accident was the gusting
crosswind conditions.
= = =
Accident occurred Saturday, May 12,
2001 in San Diego, CA
Probable Cause Approval Date:
3/30/2004
Aircraft: Gulfstream Aerospace G-IV,
registration: N999GP
Injuries: 13 Uninjured.
The main rotor blade from a
helicopter collided with the right
wingtip of a twin-engine transport
airplane while it was being
marshaled into a ramp area for
parking. The helicopter was parked
with its rotor blades aligned with
its longitudinal axis, and was being
loaded with passengers while the
airplane was being marshaled onto
the ramp area. Four ramp personnel
were utilized at the time of the
accident; three for the airplane,
and one for the helicopter. The ramp
person assisting the helicopter
stated he escorted the passengers to
the helicopter and the pilot loaded
the helicopter and closed the door.
The other three ramp personnel were
positioned around the airplane, one
at the nose and one on each wing. As
the airplane's cockpit passed abeam
the helicopter, the captain noticed
the main rotor blades start to
rotate. The airplane's first officer
was concerned with the distance
between the airplane's right wing
and the helicopter, but received a
"thumbs
up" signal from the right wing
walker.
The National Transportation Safety
Board determines the probable
cause(s) of this accident as
follows:
the failure of the ground personnel
to maintain clearance between two
aircraft on the ramp, while one
airplane was taxiing and the other
was standing with the engine running
and rotor blades turning.
= = =
Accident occurred Wednesday,
February 21, 2001 in San Diego, CA
Probable Cause Approval Date:
1/23/2002
Aircraft: McDonnell Douglas 600N,
registration: N606BP
Injuries: 2 Uninjured.
During the landing slide, the main
rotor blew back, contacted the tail
boom, and severed it. The flight
purpose was refresher training and
the specific maneuver at the time of
the accident was training in the
procedure for a stuck (fixed) right
pedal. According to the flight crew,
there were no mechanical
discrepancies with the helicopter. A
run-on landing with the fixed right
pedal was made to the 260-degree
taxiway. The wind reported at the
airport about 14 minutes after the
accident was 330 degrees at 6 knots.
The pilots reported that the wind
was 310 degrees at 6 to 8 knots with
gusts to 12 knots. According to
information provided by the flight
crew, the training pilot
accomplished the maneuver: aligned
with the runway heading with an
airspeed between 55-65 knots; the
instructor pilot (IP) held right
pedal to induce a 10-degree right
yaw; touchdown was estimated to
occur about 30-40 knots; the low
rotor rpm horn was "on" at or near
touchdown, but the
rotor speed was not noted; the
collective was positioned at some
point above half travel; cyclic was
slightly forward of neutral; shortly
after touchdown both pilots felt the
main rotor strike the tail boom;
directional control was lost and the
helicopter rotated about 220 degrees
nose right before coming to rest,
upright. The manufacturer indicated
that main rotor/tail boom contact
from blowback of the main rotor may
result from forward velocity and
low/decaying main rotor rpm (advance
ratio) due to a high collective
position during the ground run-out
phase following the 30-knot plus
touchdown. The blowback condition is
exacerbated by the high angle pitch
setting which causes blade stall
over a large portion of the rotor
disk. A blowback condition is
present in all helicopters. It may
be more pronounced in the MD600N
(versus the 500N) due to greater
helicopter gross weight, reduced
flare/deceleration capabilities
because of tail boom length and
installation angle, and the
increased surface of the additional
main rotor blade resulting in a more
rapid decay of main rotor rpm. A
caution in the helicopter's
Rotorcraft Flight Manual specifies
for practice autorotation landings
to avoid conditions of ROTOR RPM
(Nr) less than 60 percent with
headwinds across the rotor greater
than 30 knots during touchdown
autorotations. These conditions
during touchdown and subsequent
ground slide, can lead to excessive
rotor blowback, reduction in blade
tip to tail boom clearance, and
subsequent damage to the aircraft.
Avoid these conditions by reducing
collective pitch after touchdown
(surface conditions permitting) and
minimizing ground run.
The National Transportation Safety
Board determines the probable
cause(s) of this accident as
follows:
The student pilot's improper use of
the rotorcraft flight controls, and
the instructor pilot's inadequate
supervision of the maneuver.
= = =
Accident occurred Monday, December
11, 2000 in SAN DIEGO, CA
Probable Cause Approval Date:
5/28/2002
Aircraft: Cessna 172H, registration:
N4959R
Injuries: 2 Serious.
The pilot filed a visual flight plan
to practice night landings. He
contacted the tower about 1930, when
approximately 5 miles west of the
airport, and reported inbound for
touch-and-go landings. The pilot was
instructed to enter a right downwind
for runway 26R, and to change to the
correct frequency. The pilot said he
did not have the current Automated
Terminal Information Service (ATIS)
for weather information, and was
given the current weather after he
changed frequencies. The controller
noticed the airplane just west of
"Poggi" VOR (2.3 nautical miles
north of the runways), and it
appeared to be headed northbound
away from the airport. The
controller asked the pilot if he had
the airport in sight and he
responded he did not, but that he
was practicing some maneuvers and
was a little busy in the cockpit. A
couple of minutes later the airplane
was observed to be about 7 miles
north. The controller advised the
pilot to report the prison if he was
still
inbound for a right base entry for
runway 26R. The next readable
transmission from the airplane was
"encountering some soup." According
to the operator, upon entering
clouds, the pilot started a 75 mph
climb, followed by a right turn just
before impact. The pilot did not
respond to additional calls from the
controller and was no longer
observed on the D-Brite radar
system. The airplane had collided
with a 2,791-foot mountain about 7
miles north of the intended airport.
According to VFR charts, the maximum
elevation figure for the accident
quadrangle/sector is 4,100 feet mean
sea level.
The National Transportation Safety
Board determines the probable
cause(s) of this accident as
follows:
The pilot's inadequate preflight
planning and weather evaluation that
resulted in the inadvertant entry
into instrument meteorological
conditions while conducting visual
flight. A factor was fog and the
night visual conditions.
= = =
Brown Field
Airport Approach / Landing: