Gillespie Field Airport, San Diego/El Cajon, CA
Airport
Location : Gillespie Field is located 10 miles north east
of San Diego, California.
Airport
History :
In 1942 the
United States Marine Corps chose a 688-acre
(2.78 km2) site east of
San
Diego to conduct parachute training for the
newly forming
Parachute battalions. In September 1942 Camp
Gillespie was completed and named in honor of
Lieutenant
Archibald H. Gillespie, a Marine officer who
played a prominent role in the effort to separate
California from
Mexico
in the 1840s.
In February 1944, the camp was commissioned as
Marine Corps Auxiliary Airfield Gillespie falling
under the command of
Marine Corps Air Station El Toro. MCAAF
Gillespie soon became responsible for
Camp Pendleton Outlying Air Field. Among the
units that transited and trained at MCCAF Gillespie
were
VMSB-141, Air Warning Squadron 10 and the
Navy's
VT-37.
Overhead view of MCAAF Gillespie in June 1944.
In 1946, the airfield was turned over to
San Diego County and was turned into a general
aviation facility.
In 1952, the County granted ownership of the
facility by the federal government. In 1971, the
County Sheriff stationed
ASTREA, a helicopter law enforcement base at the
airport. And in 1993, the San Diego Aerospace Museum
located its restoration operations and a special
exhibit at the field.
Gillespie Field Airport Today: Obstructions
reported; Tall fences 8'. Banner Towing; Gyrocopters; Helicopter
operations;
Airport
Services and Amenities: Advanced Aircraft
Electronics; American Aviation Academy; California Flight Academy; El Cajon
Flying Service; Golden State Aviation/Golden State Flying Club; Instrument
Overhaul Avionics; Jeans Flight Training; JET Air FBO; Plus One Flyers,
Inc.; Rison Aviation; SAA Flight Training; Safari Aviation; San Diego
Aircraft Sales; Take Flight San Diego;
Special Events:
Balboa Park; Casino; Commemorative Air Force Museum; SD Aerospace Museum on
field; Wild Animal Park; Zoo; Sea World;
Airport Area Accident History:
June 2, 2010 - The small aircraft came to rest on a portion of Cuyamaca
near the west end of Gillespie Field. The downed trolley wires ignited a
small vegetation fire along the fence bordering the airport. Fire Department
personnel worked to quickly extinguish the fire while attempting to
extricate the pilot from the aircraft. SDG&E together with Metropolitan
Transit System (MTS) staff shut down power to the Santee portion of the
trolley, allowing rescue personnel to remove the pilot.
The 79 year old Del Mar pilot was the only occupant of the airplane. He
suffered non-life threatening injuries to both arms and was transported to
the hospital. The aircraft was based out of Gillespie Field and used for
training and rentals. The FAA responded to the scene to conduct an
investigation. Cuyamaca Street between N. Marshal and Prospect will remain
closed until the early evening hours while MTS works to restore the damaged
trolley cable.
Accident occurred Thursday, June 26, 2008 in El
Cajon, CA
Probable Cause Approval Date: 8/28/2008
Aircraft: Cessna 172N, registration: N6360D
Injuries: 2 Uninjured.
During a dual instructional flight, while over a
reservoir, the certified flight instructor (CFI)
simulated an engine failure by retarding the
throttle. After about 1 minute of procedures at
idle, the CFI applied power, but the engine did not
respond. The CFI performed a forced landing to a
field on a ranch. During landing, the left wing tip
struck the ground, and the left wing sustained
structural damage. The engine operated normally
during a post accident test run. The temperature and
dew point at the nearest reporting point about 6
nautical miles from the accident site near the time
of the accident were recorded as 75 degrees
Fahrenheit and 55 degrees Fahrenheit, respectively.
Plotting these values on a carburetor icing
probability chart indicated that the airplane was
operating in the range for serious icing at glide
power. According to the operator, the CFI did not
apply carburetor heat prior to retarding the
throttle during the simulated engine
failure.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The loss of engine power due to carburetor ice
resulting from the flight instructor's failure to
use the carburetor heat when simulating an engine
failure. Contributing to the accident were the
carburetor icing weather condition and the lack of
suitable terrain for the forced landing.
= = =
Accident occurred Tuesday, April 01, 2008 in El
Cajon, CA
Probable Cause Approval Date: 4/30/2008
Aircraft: Cessna 152, registration: N64938
Injuries: 1 Uninjured.
The student was on a solo flight to practice
touch-and-go landings. He said he made six
successful landings, but noticed that the winds were
increasing. On the seventh approach, the winds were
variable and started to gust. The student said that
he maintained 55 knots as he came over the approach
end of the runway. The airplane suddenly drifted to
the left side of the runway. He used ailerons, and
corrected to the centerline. The airplane touched
down hard, and bounced. After the airplane came to
rest, he saw smoke and fire, and evacuated from the
airplane.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the student pilot's inadequate compensation for
gusty, crosswind conditions, and failure to maintain
an adequate airspeed.
= = =
Accident occurred Sunday, February 17, 2008 in El
Cajon, CA
Probable Cause Approval Date: 3/31/2008
Aircraft: Piper PA-22, registration: N3316A
Injuries: 2 Uninjured.
The private pilot was with a certified flight
instructor (CFI) on a tail wheel familiarization
flight. While en route to the airport they
experienced a loss of radio communications. The
pilot set his transponder to 7600, overflew the
field at pattern altitude, and received a green
light from the tower. He entered the pattern and
started his final approach at 70 knots with one
notch of flaps, which was how the airplane was
configured for his previous landings. On short final
the CFI called for full flaps. As the flaps were
moved to the full position, airspeed decreased and
the rate of descent increased. The pilot added power
and lowered the nose in an attempt to maintain the
glide slope. At 15 to 20 feet agl the airplane began
to settle, and then bounced during touchdown. The
CFI called for the pilot to close the throttle, and
the airplane bounced a second time. The airplane
swerved left, the CFI applied right rudder, the
airplane then swerved right, and
the pilot and CFI applied left rudder and left
brake. The plane continued to perform a ground loop
to the right and the left wing dug into the terrain,
causing substantial damage to the wing structure.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The failure of both pilots to maintain directional
control during landing and the flight instructor's
inadequate supervision of the flight.
= = =
Accident occurred Friday, December 14, 2007 in El
Cajon, CA
Probable Cause Approval Date: 1/31/2008
Aircraft: Cessna 172S, registration: N567SP
Injuries: 1 Uninjured.
The student pilot stated that she was practicing
touch-and-go takeoffs and landings during her second
solo flight. She completed three uneventfully. On
the fourth one, her approach speed was higher than
normal. She landed the airplane and rolled out on
the runway. When she attempted to turn onto a
taxiway, the airplane was going too fast, and she
taxied off of the runway and into a ditch. The
outboard 2 feet of the left wing was curved upward,
and the right horizontal stabilizer and elevator
were bent.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The excessive speed while turning off of the runway
which resulted in a loss of aircraft control. The
ditch was a factor.
= = =
Accident occurred Saturday, October 06, 2007 in El
Cajon, CA
Probable Cause Approval Date: 8/28/2008
Aircraft: Yakovlev YAK-50, registration: N509RA
Injuries: 2 Uninjured.
Four Yakovlev YAK-50 airplanes were conducting a
formation flight. The number four airplane (N509RA)
was landing on the right side of runway 27R in a
staggered pattern behind the number three airplane
(N950MS). During the landing roll, the number four
airplane's propeller and right wing leading edge
struck the tail section of the number three
airplane. The number four airplane had floated and
landed past his intended landing point due to gusty
winds. The number three airplane had crossed onto
the right side of the runway during his touchdown
and landing roll due to the crosswinds. The number
four airplane slowed to a taxi speed after landing
and began a left turn onto the taxiway. The pilot of
the number four airplane did not see the number
three airplane until the propeller of his airplane
impacted the tail section of the number three
airplane.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The inadequate visual lookout of the pilot and his
failure to maintain clearance from a taxiing
airplane.
= = =
Accident occurred Friday, July 13, 2007 in El Cajon,
CA
Probable Cause Approval Date: 3/31/2008
Aircraft: Piper PA-28-181, registration: N38137
Injuries: 2 Fatal.
Radar data disclosed that the pilot flew the
airplane from the departure airport toward the
accident site, with the last recorded target at 610
feet above ground level (agl) over rising
mountainous terrain. The floor of the radar coverage
in the area was about 200 feet agl. The accident
site was located at an elevation of about 2,293 feet
mean sea level (msl) on the slope of a bowl-shaped
box canyon about 25 nautical miles (nm) from the
departure airport. In character, the canyon and
surrounding hills were steeply sloped, averaging
between 60 to 80 degrees, with the tops of the
canyon terrain about 700 feet higher than the
accident site elevation and 1,000 feet laterally in
front of the wreckage. An analysis of the airplane's
climb performance capability found that a lateral
distance of 2 miles would be required to climb 700
feet. Ground scar analysis, impact signatures, and
wreckage fragmentation patterns disclosed that the
airplane impacted in a
descending steep vertical nose down attitude
traveling downslope. The impact geometry was
consistent with the airplane encountering an
accelerated stall while attempting a course reversal
in the canyon. The width of the canyon immediately
surrounding the wreckage measured about 1,250 feet.
With a turn radius of 637.5 feet, and airspeed of 99
knots (maneuvering speed), the bank angle required
for the airplane to complete a 180-degree turn was a
minimum of 55 degrees. According to stall speed
versus angle of bank data, the stall speed would be
55 knots at 55 degrees of bank. No evidence of
mechanical malfunction or failure was found during a
post accident examination of the airplane and
engine. The pilot had accumulated 75 hours total
flight experience, of which about 2 hours was in the
same make and model as the accident airplane and
acquired in the location of the departure airport.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's inadequate in-flight decision to attempt
low altitude flight operations into a box canyon in
mountainous terrain, and his failure to maintain an
adequate airspeed while maneuvering to reverse
direction, which led to an accelerated stall and
spin.
= = =
Accident occurred Friday, March 16, 2007 in El
Cajon, CA
Probable Cause Approval Date: 6/27/2007
Aircraft: Caywood Long-Ez, registration: N829CL
Injuries: 1 Uninjured.
The airplane veered off the runway after touchdown
and damaged the landing gear structural attach
points and the fuselage. The pilot said that just
after touchdown the plane swerved left. He applied
the right brake in an attempt to correct the swerve.
The airplane departed the runway to the left and the
left main landing gear dug into the dirt, causing
damage to the main mount and fuselage. The pilot
stated that the airplane and engine had no
mechanical failures or malfunctions.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's failure to maintain directional control
of the airplane during the landing roll.
= = =
Accident occurred Tuesday, June 27, 2006 in El
Cajon, CA
Probable Cause Approval Date: 10/3/2006
Aircraft: Beech 76, registration: N6720T
Injuries: 2 Uninjured.
The airplane's left main landing gear collapsed
during the landing rollout. After performing
maneuvers in the practice area, the flight
instructor and student proceeded to a nearby airport
to practice touch-and-goes. As they approached the
airport traffic pattern, the student pilot moved the
gear selector to the down position. Once the gear
was down they noticed that the left main gear down
light was not illuminated. They recycled the landing
gear, but still received the same indication. A low
approach and flyby past the tower confirmed that the
gear was in the down position. The instructor
decided to return to his home airport instead of
landing at this airport. While en route, the
instructor and student inspected the light bulbs of
the indicator light and found them to be operating
properly. They recycled the gear one more time.
While doing this, the gear motor circuit breaker
popped, and they smelled smoke in the cockpit. They
pulled the landing gear
circuit breakers immediately and the smoke smell
cleared. The pilots extended the landing gear using
the manual extension checklist. Once the gear came
down, they still had the same unsafe gear
indication. The instructor yawed the airplane in an
attempt to lock the gear, but received the same
unsafe indication. Upon arriving at his home
airport, the instructor touched down using a
soft-field landing technique. As the airplane
decelerated, the left main landing gear collapsed
and the left wing tip and the propeller struck the
runway. Federal Aviation Administration inspectors
examined the main landing gear after the accident.
They found the left main landing gear "A" frame tube
had failed. Airworthiness Directive 97-06-10
requires repetitive inspection of the main landing
gear "A" frame assemblies for cracks and
lubrication, and requires the replacement of any
assembly found cracked. The actions specified in
this AD are intended to prevent main landing
gear failure and collapse because of a cracked "A"
frame assembly. A review of the aircraft records
indicated that AD 97-06-10 had been complied with
during the last 100-hour inspection on June 21,
2006. This aircraft is operated by a flight school
and the maintenance records show that it is operated
at an activity level where a 100-hour inspection is
accomplished once every 30 days or so.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the failure of the "A" frame tube, which caused the
left main landing gear to collapse.
= = =
Accident occurred Sunday, March 05, 2006 in El
Cajon, CA
Probable Cause Approval Date: 10/31/2006
Aircraft: Piper PA-24, registration: N6094P
Injuries: 1 Uninjured.
The solo student pilot was practicing touch-and-go
landings on a dry, paved runway. He said that after
landing, as he applied full engine power for
takeoff, the airplane veered to the left and
continued off the left side of the runway. He
aborted the takeoff, but the airplane's right main
wheel struck a sign post and the right main landing
gear collapsed. The airplane's right wing struck the
ground, and sustained substantial damage. The
student pilot noted that there were no preaccident
mechanical anomalies with the airplane.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The student pilot's failure to maintain directional
control during takeoff, which resulted in an on
ground collision with a sign, and the collapse of
the main landing gear.
= = =
Accident occurred Wednesday, February 08, 2006 in El
Cajon, CA
Probable Cause Approval Date: 3/26/2007
Aircraft: Cessna 172RG, registration: N9531B
Injuries: 3 Fatal.
A Cessna 182Q and a Cessna 172RG, were operating in
class D airspace and departed from the same airport.
The Cessna 172RG was operating under instrument
flight rules as an instructional flight (IFR) and
receiving radar service from an approach control
facility, while the Cessna 182 was operating under
visual flight rules (VFR) and had been released from
communication with air traffic control. The pilot
undergoing instruction in the Cessna 172RG was most
likely wearing a view limiting device which tasked
the certified flight instructor seated in the right
seat to serve as both an instructor and a safety
pilot. The Cessna 172RG departed first, performing a
right 260-degree turn over the airport and was
assigned a southwest heading by the controller. The
Cessna 182Q departed to the west and made a left
turn, while climbing in a southeasterly direction.
The heading assigned to the Cessna 172RG put it on a
direct collision course with the Cessna 182Q, with a
collision angle of 40 degrees. Following a
discussion with the controller about the pilot's
intentions upon completion of an approach, the
controller instructed the Cessna 172RG to fly
heading 190. The pilot read back, "One nine" and no
further transmissions were received from the Cessna
172RG. In class D airspace, there is no specified
separation requirement between VFR and IFR aircraft.
However, controllers still have a responsibility to
be vigilant for potential collisions between
aircraft under these circumstances. This accident
occurred after the controllers in communication with
the Cessna 172RG had received a sustained conflict
alert involving the Cessna 172RG and Cessna 182Q
(operating on a VFR transponder code), but failed to
recognize or resolve the conflict. Comparisons of
the calculated convergence angles of the two
airplanes showed that for an 85th percentile male
seated in the left seat (Cessna did not create pilot
view angles for pilots
seated in the front right seat), the Cessna 172RG
pilot was about 15 degrees outside of the right view
angle and the Cessna 182Q pilot was within about 6
degrees of the left view angle.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilots of both airplanes failure to maintain an
adequate visual lookout due to their relative flight
paths, which limited the available visuaAccident
occurred Tuesday, December 13, 2005 in El Cajon, CA
Probable Cause Approval Date: 3/28/2006
Aircraft: Grafton Rand KR-1, registration: N47186
Injuries: 1 Uninjured.
The airplane struck a taxiway light after landing.
The pilot said he turned left onto the taxiway with
excessive speed, lost control of the aircraft, and
struck a taxiway light with the right wing tip. The
impact damaged the wing and broke the landing gear
lock, which caused the right main landing gear to
collapse.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's attempt to turn off the runway at an
excessive taxi speed.l cues. Factors were the
failure of the air traffic controller(s) to issue a
conflict
= = =
Accident occurred Wednesday, January 12, 2005 in El
Cajon, CA
Probable Cause Approval Date: 3/28/2006
Aircraft: Jimmy Hill Lancair 235, registration:
N124JH
Injuries: 1 Fatal, 1 Serious.
The airplane collided with an airport boundary fence
about 500 feet short of the runway's approach end
while on final approach for landing. A witness
driving a pickup truck said that she saw the
airplane cross in front of her truck about 10 feet
above the ground going very fast and low.
Immediately after the airplane crossed her path, it
struck the airport boundary fence with its right
main landing gear and impacted the dirt terrain
beyond. The wreckage was about 500 feet from the
approach end of the runway, and about 1,800 feet
from the runway's displaced threshold. The passenger
of the airplane said that this was her first flight
with the pilot. She recalls that the flight was very
pleasant, and the pilot did not express any concerns
regarding the airplane or the environment. As they
approached the runway for landing the pilot said to
her "Do you see the runway? I will reduce some power
for landing." Moments after that statement the
airplane collided
with the airport boundary fence. Examination of the
airplane revealed no evidence of a preimpact
malfunction or failure of the control system or
power plant.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's failure to maintain the proper glidepath
to avoid obstacles and terrain.
= = =
Accident occurred Saturday, October 11, 2003 in El
Cajon, CA
Probable Cause Approval Date: 12/30/2003
Aircraft: Avions Max Holste MH 1521 BROUSSARD,
registration: N239HL
Injuries: 1 Uninjured.
The airplane stalled during the takeoff initial
climb. After an expedited takeoff and 3 seconds into
the takeoff roll, the pilot applied forward stick to
raise the tail. After 5 seconds, the tail was still
on the ground. He then moved his left hand to the
stick so that he could use his right hand to apply
nose down trim. However, before he could apply it
and prior to attaining takeoff airspeed, the
airplane ballooned about 8 feet into the air. As it
re-contacted the ground, the airplane bounced and the
right wing stalled. The right wing impacted the
ground, followed by the left main gear, and then the
left wing tip. The propeller contacted the ground as
the left main gear hit, and the engine stopped. The
pilot did not report any mechanical problems with
the airplane. The pilot reported that he took off
prior to reaching takeoff airspeed and stalled the
airplane. He felt that additional nose down trim
could have prevented the accident.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's premature liftoff and his failure to
attain an adequate takeoff airspeed, which resulted
in a stall. The pilot's failure to correctly set the
pitch trim before takeoff was a factor.
= = =
Accident occurred Thursday, April 03, 2003 in El
Cajon, CA
Probable Cause Approval Date: 9/1/2004
Aircraft: Vortec 99, registration: N6052T
Injuries: 1 Uninjured.
The airplane collided with ground obstacles during a
forced landing following a loss of engine power.
Prior to flying the experimental airplane, the pilot
had done some work on the airplane's Chevrolet,
4.3L, V6 engine. The pilot was performing a test
flight at pattern altitude over the airfield when
the engine began to "run rough and quit." During the
forced landing approach to the runway, the pilot
executed an approach that put him on a low final for
landing. The airplane landed short of the runway,
struck a fence post, and came to rest in the
threshold area of the approach end of runway. The
cause of engine failure was not determined.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
A loss of engine power for undetermined reasons.
alert to the Cessna 172RG after repeated visual and
aural warnings of an impending collision and the
task load of the certified flight instructor.
= = =
Accident occurred Sunday, February 23, 2003 in El
Cajon, CA
Probable Cause Approval Date: 10/28/2004
Aircraft: Luscombe T-8F, registration: N1822B
Injuries: 2 Uninjured.
During landing rollout, the airline transport pilot
encountered a left crosswind, lost directional
control, collided with a sign, applied engine power
thereby initiating a go-around and finally collided
with terrain. Previously, the second pilot had
performed three takeoffs and landings in the traffic
pattern. The certificated airline transport pilot
(ATP) performed the fourth landing on runway 27R.
During rollout he pulled the control stick aft and
left. The airplane veered left, directional control
was lost, and the airplane collided with a taxiway
sign. Thereafter, the ATP applied full engine power
to go around. The airplane veered right, exited the
right side of the runway, and became airborne. While
in ground effect, the airplane's right wing tip
impacted a nearby dirt embankment. The airplane came
to rest in a grassy field on airport property. The
ATP indicated that during the attempted landing the
left crosswind increased in speed and a gust was
encountered. He estimated that the wind was from 220
degrees at 10 knots, with an occasional gust to 14
knots.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's inadequate compensation for the
crosswind conditions and loss of directional control
during landing.
= = =
Accident occurred Tuesday, September 17, 2002 in El
Cajon, CA
Probable Cause Approval Date: 9/29/2004
Aircraft: Cessna 152, registration: N5100B
Injuries: 1 Uninjured.
The airplane touched down hard in a nose low
attitude buckling the firewall and collapsing the
nose gear assembly. The pilot said the accident
occurred while he was attempting to land at the
conclusion of his practice flight and that he
"flared too high," and then the airplane's nose
dropped. The airplane contacted the runway and
bounced several times before coming to rest. No
pre-impact mechanical problems were experienced with
the airplane.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's misjudged landing flare, which resulted
in a hard landing.
= = =
Accident occurred Saturday, May 11, 2002 in El
Cajon, CA
Probable Cause Approval Date: 6/2/2004
Aircraft: Ercoupe (Eng & Research Corp.) 415C,
registration: N2948H
Injuries: 1 Serious.
After flying for about an hour, the engine lost
power and the airplane collided with obstacles and
the ground on a freeway during an attempted forced
landing. The recently overhauled engine had just
been installed the morning of the accident in the
airframe and this was the first flight following
this maintenance activity. The mechanic who
installed the engine said after he completed the
reinstallation he performed a 20-minute ground run
of the engine. A fuel leak was noted in a fitting in
the line to the carburetor and that was tightened.
There were no other discrepancies noted in the
engine indications. The pilot arrived at the airport
after the mechanic had performed the ground run of
the engine. He said the mechanic told him that the
airplane was ready for a test flight and that he
should take it up for about an hour to break-in the
engine, changing the rpm setting every 5 minutes.
The pilot said he did a preflight inspection, which
included the
determination that he had 6 gallons in each of the
wing tanks and 6 gallons in the header tank, for a
total of about 18 gallons. After the preflight, he
started the engine and taxied down to the runway
where he did his normal run-up process, which
included two separate magneto checks. After takeoff
he flew out about 3 miles and orbited while varying
the rpm every 5 minutes. During the entire flight
from engine start, the power plant performed
perfectly with no abnormal engine indications. At
the end of 1 hour, he reported to the control tower
that he was ready to land and turned inbound toward
the runway. On final approach, the engine just quit
without any precipitating roughness or engine spool
down. He said it was "like someone just turned off
the key." He did not have enough altitude to make
the runway and the airplane hit a fence and landed
inverted on the highway. Post accident examination
of the engine and related systems found numerous
discrepancies and abnormal conditions related to the
engine overhaul and its reinstallation in the
airframe. While many of these discrepancies would
have eventually induced a catastrophic engine
failure, they were not contributory to the loss of
engine power. Three specific conditions were likely
related to the engine power loss. The engine driven
fuel pump's outlet fitting was found loose and was
easily moved, and the nuts attaching the fuel pump
to the crankcase were found to be only finger tight.
The nuts securing the P-leads for both magnetos were
loose, with the nuts 2-turns from finger tight. The
scuffing on the pistons indicates that the overhaul
shop did not pre-oil the pistons, rings, and
cylinders when the engine was put back together;
this dry condition allowed a large quantity of oil
to migrate past the rings, fouling the plugs with
carbon deposits. The fuel system in the aircraft
consists of a 6-gallon tank in each wing and a
6-gallon
header tank, which is mounted in front of the
cockpit. Fuel is supplied to the engine's carburetor
via gravity fed line only from the header tank. The
engine driven fuel pump moves fuel from the wing
tanks to the header tank to replenish that supply as
the engine uses it. According to the Teledyne
Continental operating manual for the "C" series
engines, the typical cruise fuel consumption rate of
the C75 engine is between 5 and 6 gallons per hour.
At the conclusion of the impact sequence, the
aircraft came to rest inverted, with all three fuel
tanks breeched. A fuel spill was noted under the fuel
tank locations in both wings, and based on the size
of the fuel stain, investigators estimated at least
10 gallons had leaked. The loose fitting on the fuel
pump likely allowed it to suck air and resulted in
inefficiency to the extent that the header tank was
depleted of fuel, which in turn resulted in a fuel
starvation event. The mechanic was going to leave
town immediately after completing this job for a
planned multi week vacation trip.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
fuel starvation due to the mechanic's failure to
properly tighten a fuel line fitting on the engine
driven fuel pump, which led to a depletion of the
fuel in the header tank. The mechanic's self induced
pressure to complete the job prior to leaving on
vacation was a factor in the accident.
= = =
Accident occurred Sunday, June 24, 2001 in El Cajon,
CA
Probable Cause Approval Date: 10/24/2002
Aircraft: Stolp Starduster SA-300, registration:
N711MH
Injuries: 2 Uninjured.
The pilot was becoming familiar with the
experimental airplane because he intended to
purchase it from the pilot-rated passenger. During a
touch-and-go landing, the pilot applied too much
rudder, and he lost directional control. When the
airplane veered off the runway the lower left wing
contacted the ground and broke.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's failure to maintain directional control
during landing rollout.
= = =
Accident occurred Tuesday, October 03, 2000 in EL
CAJON, CA
Probable Cause Approval Date: 11/6/2001
Aircraft: Aerospatiale AS350BA, registration: N189ND
Injuries: 2 Uninjured.
While positioning the helicopter from the ground to
a storage cart, the pilot lost directional, made a
hard landing, and the tail boom struck the ground.
Prior to the loss of directional control, the pilot
saw something depart the tail section. He attributed
the loss of directional control to a tail rotor
failure. He initiated an autorotation over the
landing cart. He maneuvered away from the cart in
order to land on the ground and prevent a partial
landing on the cart. The on-scene investigation
revealed the aft drive shaft coupling was detached
from the tail rotor drive shaft. Three bolts retain
the coupling. One bolt was found attached to the
coupling, another bolt was found on the ground, and
the third bolt, and two of the retaining nuts, were
not located. Neither bolt exhibited stripped threads
or deformation. The last maintenance performed on
the helicopter was by the previous owner. A track
and balance of the tail rotor system was performed
about
48 flight hours prior to the accident. According to
the manufacturer's maintenance instructions, the
balancing is accomplished by placement of washers
under the nuts that are used to secure the bolts
that attach to the aft drive shaft coupling. These
are the same nuts that were not located at the
accident site. Maintenance instructions also specify
that the bolts in this area should be checked for
proper torque and safety after an inspection.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
Improper torquing procedure of the aft tail rotor
drive shaft coupling by maintenance personnel after
tracking the tail rotor.
Accident occurred Sunday, December 31, 2006
in
San Diego, CA
Probable Cause Approval Date: 3/31/2008
Aircraft: Cessna 150J, registration: N50814
Injuries: 1 Fatal.
During a banner pickup maneuver between two
poles, witnesses saw the airplane approach
the poles at the correct altitude with the
flaps extended as prescribed; however, it
appeared to be flying at a slower than
normal speed for the pickup. Procedures
dictate that just before the airplane
reaches the pickup poles, the pilot is
supposed to apply full power, and pitch the
nose of the airplane up approximately 45
degrees to swing the hook into the towline
strung between the pickup poles. As the
airplane reached the poles, the engine noise
did not increase and the airplane did not
pitch up enough initially to capture the
towline, but it did pitch to the correct
45-degree angle seconds after the miss. The
engine power did not increase as the
airplane continued to climb until it
stalled, and then rolled over to the left
into the ground. Investigators noted no
preimpact anomalies with the engine, engine
controls, or airframe.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The pilot's improper use of the throttle and
failure to maintain an adequate airspeed
that resulted in a stall/spin.
= = =
Accident occurred Sunday, November 27, 2005
in San Diego, CA
Probable Cause Approval Date: 4/25/2007
Aircraft: Cessna 182A, registration: N3936D
Injuries: 1 Uninjured.
The engine experienced a loss of power and
the airplane collided with a fence while the
pilot was performing a forced landing. As
the airplane approached the vicinity of the
destination airport, the engine experienced
a total loss of power. The pilot made a
forced landing on highway about 2 miles from
the airport. During
the landing roll, the airplane
impacted a fence. A post accident
examination of the engine revealed that
rotation of the crankshaft did not generate
rotation of the camshaft. Removal of the
starter drive gear assembly revealed that
four gear teeth were missing from the
camshaft sprocket and one gear tooth was
missing from the crankshaft sprocket. The
gear teeth were retrieved and sent to the
Safety Board Materials Laboratory for
examination. The camshaft gear sprocket
failed due to fatigue initiating at the root
of one of the teeth. Several other teeth had
fatigue consistent with secondary initiation
due to load shedding from the
original failed tooth; the crankshaft gear
failure was also secondary. Micro-structural
examination and hardness testing was
performed on a section of a camshaft tooth,
which met drawing specifications. A thin
layer of decarburization was observed on the
surface.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The failure of the camshaft due to fatigue
of one of the gear teeth, which resulted in
a loss of engine power. Factors were the
fence and the fence post.
= = =
Accident occurred Saturday, July 30, 2005 in
San Diego, CA
Probable Cause Approval Date: 8/29/2006
Aircraft: Cessna 210A, registration: N9468X
Injuries: 1 Uninjured.
The partially extended landing gear
collapsed during rollout on the runway. No
evidence of a mechanical malfunction was
noted with the landing gear system during
the pilot's flight. The pilot said that on
approach he was distracted while looking for
another airplane, and he did not observe
whether the green gear down light was
illuminated after he extended the landing
gear. He increased engine power in
anticipation of performing a go-around, then
located the other airplane, whereupon he
closed the throttle and landed. Seconds
later during rollout, the airplane's landing
gear collapsed. Airport management reported
that the airplane was subsequently hoisted
up by a crane, the landing gear was manually
extended into the locked position, and the
airplane was rolled off the runway. The
landing gear extension system and the
related gear warning horn were functionally
examined after the accident with no
anomalies found.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The pilot's failure to ensure that the
landing gear was fully extended prior to
landing. A contributing factor was the
pilot's diverted attention.
= = =
Accident occurred Saturday, July 07, 2001 in
San Diego, CA
Probable Cause Approval Date: 11/28/2001
Aircraft: Sparks KR-2, registration: N122MS
Injuries: 1 Uninjured.
The pilot, who was the original owner and
builder of this aircraft, stated that while
he was decelerating during his landing
rollout, he encountered a gust of wind from
the left, which caused the airplane to
become airborne again with the left wing
high. He added power and avoided a stall,
but had drifted off the runway. The left
main landing gear hit a runway light,
causing the airplane to
ground loop, which damaged the
outboard 2 feet of the left wing. The pilot
stated that he would repair the wing and fly
the airplane again. He stated that the
damage was easy to repair and woud take only
a few days to complete. According to the
pilot, he had approximately 2,000 hours of
flight time, 700 of which was in the
accident airplane. He had logged 50 hours in
this airplane within the last 90 days. When
asked how he could prevent this accident
from happening in the future, he stated
"Don't go flying."
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
Failure of the pilot to maintain directional
control during landing.
= = =
Accident occurred Tuesday, September 05,
2000 in SAN DIEGO, CA
Probable Cause Approval Date: 10/17/2001
Aircraft: Williams WILLIAMS MITE M18L,
registration: N60BW
Injuries: 1 Uninjured.
On landing approach in an experimental
airplane, the entire stabilizer and rudder
assemblies separated from the airplane, as a
single unit. Thereafter, the airplane veered
sharply to the right, and there was a strong
tendency to roll inverted. The pilot
regained control of the airplane, extended
the landing gear, and landed on runway 17
without further mishap. The separated
components were subsequently located on
airport property. A
Federal Aviation Administration inspector
examined the components and reported
observing evidence of dry rot on the
fracture surfaces.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The separation of the airplane's
vertical stabilizer and rudder
assemblies, during the landing approach,
because of dry rot.
Gillespie Field
Airport Approach / Landing: