Montgomery Field Airport, San Diego, CA
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Airport Area Accident History:
Accident occurred Tuesday, June 24, 2008 in San
Diego, CA
Probable Cause Approval Date: 7/30/2008
Aircraft: Cessna 172M, registration: N9629V
Injuries: 1 Uninjured.
The student pilot reported that he was practicing
touch-and-go landings and made a normal landing on
runway 28L. Witnesses located adjacent to the runway
observed the landing, and stated that the airplane
landed hard on the right main landing gear. During
the landing roll, the pilot raised the flaps, turned
the carburetor heat off, and started to increase
engine power when the airplane then began to veer to
the left. He then applied full engine power in an
attempt to get the airplane airborne. The airplane
became airborne and the left main landing gear
struck a taxiway sign. The pilot then elected to
abort the takeoff and he reduced engine power,
switched off the master switch and turned off the
magnetos. The airplane continued into the adjacent
ramp area and struck a parked and unoccupied
helicopter.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The student pilot's failure to maintain directional
control during a touch-and-go landing.
= = =
Accident occurred Thursday, January 11, 2007 in San
Diego, CA
Probable Cause Approval Date: 8/30/2007
Aircraft: Cessna TR182, registration: N5443S
Injuries: 1 Serious.
The airplane impacted the runway in a nose-down
attitude during the takeoff initial climb out. The
79-year old pilot was departing on a short flight to
his home airport when the accident occurred.
According to a witness, the airplane climbed to 100
feet and suddenly pitched nose-down. The airplane
continued in this attitude until ground impact. Post
accident examination of the airplane control systems
did not reveal any operational anomalies.
Investigators noted that the trim tab was set 10
degrees nose down and the flaps were extended to 40
degrees. Both of these control positions are
inconsistent with normal takeoff settings as
specified by the airplane manufacturer.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's failure to maintain control of the
airplane during takeoff. A contributing factor to
the accident was the improper takeoff configuration
of the airplane.
= = =
Accident occurred Friday, October 13, 2006 in San
Diego, CA
Probable Cause Approval Date: 2/26/2007
Aircraft: Finney Thorp T-18, registration: N467JF
Injuries: 1 Uninjured.
The airplane ground looped during the landing
rollout and the right wing was bent. The pilot
reported that the approach and touchdown were
normal, but he lost directional control during the
rollout due to crosswind conditions. The pilot
stated that there were no mechanical anomalies with
the airplane.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's inadequate compensation for the
crosswind conditions and failure to maintain
directional control during landing.
= = =
Accident occurred Sunday, November 19, 2006 in San
Diego, CA
Probable Cause Approval Date: 11/29/2007
Aircraft: Cessna 172RG, registration: N28RJ
Injuries: 4 Uninjured.
According to a report obtained from the airport
manager, the airplane experienced a complete
electrical failure during the flight. The pilot
elected to return and land at the departure airport.
After receiving a clearance to land from the tower
(via light gun signal), the pilot prepared for
landing and moved the landing gear handle to the
down position. The landing gear dropped from their
bays, but did not extend and lock into place. The
pilot did not pump the emergency landing gear
extension handle to lock the landing gear in the
down position. As the aircraft touched down on the
runway, the main landing gear legs folded back into
their retracted position. The left wing and
horizontal stabilizer contacted the runway as the
aircraft came to a stop in an upright position. The
airplane sustained substantial damage to its left
horizontal stabilizer. The reason for the electrical
failure was not determined.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
An undetermined total electrical failure. The
pilot's failure to extend the landing gear to the
down and locked position was a factor.
= = =
Accident occurred Monday, May 08, 2006 in San Diego,
CA
Probable Cause Approval Date: 7/25/2007
Aircraft: McKenzie Lancair IV-P Turbine,
registration: N5M
Injuries: 1 Uninjured.
The airplane veered off the runway after the left
main gear collapsed on landing. The pilot was
cleared to land on runway 28L. He lowered the
landing gear in preparation for landing, and
received an indication of three green lights
confirming that the gear was down and locked. At
this point, an electrical power failure occurred,
and he initiated a go-around. He turned the
emergency battery on, and this restored power to the
radio and several critical systems. The gear lights
indicated that only the nose and right main were now
down and locked. He asked the tower controller to
confirm the gear position. The tower said it
appeared to be down, and cleared the pilot to land
on runway 28R. Upon touchdown, the left main gear
collapsed. The pilot stated that he should have
tried to pump the gear in an attempt to get it in
the locked position. No determination was made
regarding the reason for the collapse of the left
main landing gear.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The collapse of the left main gear for undetermined
reasons. A factor was the pilot's inadequate
remedial action in response to the left main gear
not locked warning light by not attempting to
manually extend the gear to ensure it was fully down
and locked.
= = =
Accident occurred Monday, March 27, 2006 in San
Diego, CA
Probable Cause Approval Date: 8/29/2006
Aircraft: Claypool RV-6A, registration: N428BC
Injuries: 1 Minor.
The solo private pilot was landing on a hard
surfaced runway at the conclusion of a Title 14, CFR
Part 91 personal cross-country flight in an
experimental, amateur built airplane. He said during
landing he overshot the final approach course, and
in an attempt to salvage the landing, he forgot to
put in the last notch of flaps. He said the airplane
crossed the threshold too fast and would not slow
down. He stated that the airplane landed hard, and
then porpoised. On the third bounce, he said the
nose wheel collapsed, and the airplane nosed over.
He said he should have gone around and reconfigured
the airplane instead of attempting to land. The
pilot reported that there were no mechanical
anomalies with the airplane prior to the accident.
He said the airplane sustained structural damage to
the nose gear, wings, and fuselage.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's improper recovery from a bounced
landing, which resulted in a hard landing, the
collapse of the nose landing gear, and a nose over.
A factor associated with the accident was the
pilot's failure to perform a go-around.
= = =
Accident occurred Saturday, November 13, 2004 in San
Diego, CA
Probable Cause Approval Date: 12/28/2006
Aircraft: Great Lakes 2T-1A, registration: N502GL
Injuries: 2 Uninjured.
On the landing rollout the airplane ground looped.
The certified flight instructor (CFI) reported that
he was demonstrating a forward slip to lose altitude
for landing. As the airplane was rolling out, he
attempted to slow down by adding light pressure on
both heel brakes. The airplane began a right turn,
and he counteracted with additional pressure on the
left brake, but there was no response. The airplane
swerved off the runway and ground looped. A Federal
Aviation Administration inspector examined the
airplane's brake system. When he depressed the
brakes he found them a little spongy but completely
operational.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the flight instructor's failure to maintain
directional control during the landing rollout.
= = =
Accident occurred Friday, July 23, 2004 in San
Diego, CA
Probable Cause Approval Date: 3/28/2006
Aircraft: Cessna 172RG, registration: N5167R
Injuries: 1 Uninjured.
The right main landing gear collapsed during rollout
following a normal touchdown on the runway.
Thereafter, directional control was lost, and the
right wing struck the surface of the runway. The
airplane veered off the runway, and it came to rest
in an adjacent open dirt field. During flight the
pilot had experienced a low voltage condition, and
his radio communications became problematic as the
battery gradually discharged. The pilot cycled the
airplane's master electric system switch in
accordance with instructions in the Cessna Pilot's
Operator's Handbook. Because this did not restore
electric power, the pilot reduced the electrical
load to conserve energy. No evidence of any
mechanical malfunction was found during the post
impact examination of the landing gear and
alternator/battery electric system. During the
examination the alternator field circuit breaker was
found in the tripped position. The examination
revealed that when the alternator
circuit breaker was reset, electric current was
restored to the buss and the battery was charging.
Prior to landing, the pilot failed to properly
perform procedures relating to ensuring that the
alternator circuit breaker was engaged. Also, the
pilot failed to ensure that the landing gear was
fully extended by using the emergency gear extension
system.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's failure to ensure that the landing gear
was fully extended, by use of the emergency gear
extension system, which resulted in its partial
collapse during landing rollout. Also causal was the
pilot's failure to follow POH procedures relating to
troubleshooting and restoring electric power to the
airplane busses.
= = =
Accident occurred Sunday, January 11, 2004 in San
Diego, CA
Probable Cause Approval Date: 4/28/2004
Aircraft: Cessna 152, registration: N67844
Injuries: 1 Uninjured.
The airplane collided with a fuel truck while taxing
to parking. While taxiing on the ramp area, between
rows of parked airplanes, the pilot noticed a parked
fuel truck ahead of her on the left side. After
deciding she had adequate clearance between the
airplane and the fuel truck, she continued taxiing
and momentarily glanced down at the airplane's
checklist. She stated that she "incorrectly judged"
the distance between the airplane and fuel truck,
and the airplane struck the fuel truck with the
outboard section of the left wing. The pilot
reported no preimpact mechanical malfunctions or
failures with the airplane.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's misjudgment of clearance from the
vehicle while taxiing. A factor in the accident was
the pilot's diverted attention.
= = =
Accident occurred Sunday, October 19, 2003 in San
Diego, CA
Probable Cause Approval Date: 2/24/2005
Aircraft: Cessna 170, registration: N3979V
Injuries: 1 Uninjured.
The airplane ground looped off the runway when the
pilot's seat slid aft during landing. The pilot said
that when he flared for landing he heard a "click"
and then his seat slid backwards about 1 foot,
restricting his ability to reach the controls. The
pilot tried to adjust his seat position to regain
access to the airplane's controls, but the airplane
entered a left ground loop and came to rest left of
the runway. A Federal Aviation Administration
inspector examined and photographed the pilot's
seat. He reported that the seat track locking pin
was positioned outside the seat track. He observed
that the side floor deck was buckled, the seat was
structurally deformed, and the seat locking pin was
outside the seat rail and roller, all indicative of
impact related damage. The inspector stated that he
could not make a reliable determination of pin
position prior to the impact damage.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's inadequate preflight inspection which
failed to determine the security of his seat, and
his failure to maintain directional control.
= = =
Accident occurred Saturday, October 25, 2003 in San
Diego, CA
Probable Cause Approval Date: 3/30/2004
Aircraft: Piper PA 28-161, registration: N39494
Injuries: 2 Uninjured.
A Cessna 172R, N72AF, and a Piper PA-28-161, N39494,
collided during taxi. The left wing and the
propeller of the Piper respectively struck the
rudder and right aileron of the Cessna. According to
the pilot of the Piper, after arriving at the run-up
area, the pilot attempted to slow the airplane.
Instead of using the brake pedals, he used the
rudder pedals. The pilot closed the throttle, but
was unable to prevent the collision. The pilot did
not report any mechanical malfunctions with the
airplane.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the student pilot's inadvertent application of the
rudder pedals rather than the brakes, which resulted
in the on ground collision with the Cessna 172R.
= = =
Accident occurred Tuesday, December 09, 2003 in San
Diego, CA
Probable Cause Approval Date: 3/30/2004
Aircraft: Beech 58P, registration: N58JG
Injuries: 2 Uninjured.
The airplane collided with a parked, unoccupied,
vehicle while taxiing to the active runway. The
pilot said that while taxiing, he noticed a red
truck parked on the right side of the taxiway. He
maneuvered the airplane so that the nose gear was
about 1 foot to the left of the taxiway centerline,
and attempted to avoid the vehicle. He estimated
that he was taxiing about 7 miles per hour when the
right wing contacted the truck's cab and he felt the
airplane suddenly veer sharply to the right. The
right propeller made contact with the front of the
truck, and he applied the brakes. After the airplane
came to a complete stop, he shut down both engines.
The pilot stated that there were no preimpact
mechanical malfunctions or failures with the
airplane.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's inadequate lookout, which resulted in
his failure to maintain clearance from the vehicle
while taxiing.
= = =
Accident occurred Tuesday, December 09, 2003 in San
Diego, CA
Probable Cause Approval Date: 3/30/2004
Aircraft: Beech 58P, registration: N58JG
Injuries: 2 Uninjured.
The airplane collided with a parked, unoccupied,
vehicle while taxiing to the active runway. The
pilot said that while taxiing, he noticed a red
truck parked on the right side of the taxiway. He
maneuvered the airplane so that the nose gear was
about 1 foot to the left of the taxiway centerline,
and attempted to avoid the vehicle. He estimated
that he was taxiing about 7 miles per hour when the
right wing contacted the truck's cab and he felt the
airplane suddenly veer sharply to the right. The
right propeller made contact with the front of the
truck, and he applied the brakes. After the airplane
came to a complete stop, he shut down both engines.
The pilot stated that there were no preimpact
mechanical malfunctions or failures with the
airplane.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot's inadequate lookout, which resulted in
his failure to maintain clearance from the vehicle
while taxiing.
= = =
Accident occurred Sunday, December 14, 2003 in
Claremont, CA
Probable Cause Approval Date: 5/29/2007
Aircraft: Cessna 421C, registration: N6887L
Injuries: 1 Fatal.
The airplane impacted a residence during a missed
approach. After completing the en route portion of
the instrument flight, a controller cleared the
pilot to proceed direct to the initial approach fix
for the global positioning satellite (GPS) approach
to the airport. After being cleared for the
approach, the airplane continued on a course to the
east and at altitudes consistent with flying the GPS
published approach procedure. Radar data indicated
that at the missed approach point at the minimum
descent altitude of 2,000 feet msl, the airplane
made a turn to the left, changing course in a
northerly direction toward rapidly rising
mountainous terrain. The published missed approach
specified a climbing right turn to 4,000 feet, and
noted that circling north of the airport was not
allowed. Remaining in a slight left turn, the
airplane climbed to 3,300 feet msl over the duration
of 1 minute 9 seconds. The controller advised the
pilot that he was flying off
course toward mountainous terrain and instructed him
to make an immediate left turn heading in a
southbound direction. The airplane descended to
3,200 feet msl and made a left turn in a southerly
direction. The airplane continued to descend to
2,100 feet msl and the pilot read back the
instructions that the controller gave him. The
airplane then climbed to 3,300 feet, with an
indicated ground speed of 35 knots, and began a
sharp left turn. It then descended to impact with a
house. At no time during the approach did the pilot
indicate that he was experiencing difficulty
navigating or request assistance. An examination of
the airplane revealed no evidence a mechanical
malfunction or failures prior to impact; however,
both the cockpit and instrument panel sustained
severe thermal damage, precluding any detailed
examinations.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
the pilot became lost/disoriented during the
approach, failed to maintain course alignment with
the missed approach procedure, and subsequently lost
control of the airplane.
= = =
Accident occurred Thursday, May 16, 2002 in SAN
DIEGO, CA
Probable Cause Approval Date: 11/25/2003
Aircraft: Cessna 182Q, registration: N9031U
Injuries: 1 Uninjured.
The plane overran the runway after making a
full-stop landing. The pilot was intending to do
touch-and-go landings, but decided to make his
landing a full-stop due to the glare from the sun.
After he touched down, the glare from the sun was so
intense he had to move up in the seat, slipping his
feet off the rudder pedals. He couldn't stop the
airplane and ran off the end of the runway into a
light pole.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's failure to apply continuous brake
pressure. Sun glare is a contributing factor.
= = =
Accident occurred Sunday, March 03, 2002 in San
Diego, CA
Probable Cause Approval Date: 6/30/2004
Aircraft: Piper PA-28-140, registration: N1775T
Injuries: 1 Uninjured.
The airplane experienced a loss of engine power and
impacted terrain about 450 yards from the approach
end of the runway. The pilot spent about 1.5 hours
reviewing the flight manual for the airplane due to
his unfamiliarity with this model. He departed with
the left fuel tank selected. He spent about 2 hours
flying, and then returned to the departure airport.
On his initial descent he switched the fuel selector
valve to the right tank. About 1 nm from touchdown,
the engine began to lose power. He rechecked that
the mixture was rich, and the carburetor heat was
on. He contacted the air traffic control tower and
declared an emergency. He executed a forced landing
short of the runway due to insufficient altitude.
The pilot inspected the fuel tanks and observed no
fuel in the tanks; however, the airplane was in a
nose down, left wing low attitude. An FAA inspector
examined the fuel system. He observed fuel in the
left tank, but none in the right tank. A post
accident engine ground run-up was conducted
utilizing the left tank with no discrepancies noted.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
fuel starvation due to the pilot's mismanagement of
the fuel system.
= = =
Accident occurred Saturday, February 09, 2002 in SAN
DIEGO, CA
Probable Cause Approval Date: 10/24/2002
Aircraft: Great Lakes 2T-1A-1, registration: N502GL
Injuries: 2 Uninjured.
The airplane veered off the runway, a wheel dug into
the dirt, and the airplane nosed over. The accident
occurred on the pilot's third landing. He made a
good 3-point landing just past the numbers. During
the landing roll as the airplane slowed to 5 to 10
mph, a gust of wind hit the tail and the airplane
swerved off the runway.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot failed to maintain directional control
after encountering a gust of wind during the landing
roll. Factors were the unexpected wind gusts and the
soft terrain adjacent to the runway.
= = =
Accident occurred Wednesday, January 30, 2002 in San
Diego, CA
Probable Cause Approval Date: 10/23/2002
Aircraft: Hillyer XL-RG Velocity, registration:
C-FPDL
Injuries: 2 Fatal.
The pilot of the amateur built, experimental
airplane, contacted the military tower and said:
"... tower this is Canadian papa delta lima with an
emergency we've uh run out of fuel." The tower
controller gave the pilot the altimeter setting and
surface wind and clearance to land on the runway
nearest the pilot's position. There was a subsequent
conversation between the tower and the pilot a few
seconds later regarding the arresting gear in place
on the runway during which the pilot said: "we're
just hoping we make the runway." The tower
controller approved landing on the taxiway. The
airplane subsequently impacted an embankment about
200 feet short of the runway threshold in an open,
grassy area. An FAA inspector responded to the scene
and reported finding only a small amount of fuel
(less than 1 quart) in the aircraft. The fuel tanks
were not breached. The builder of the airplane said
it was equipped with a fuel totalizer system that
used capacitance
type fuel quantity sensors and had been carefully
calibrated and was quite accurate. Prior to the
accident flight, the builder said that he observed
the pilot use a plain, uncalibrated stick of wood to
measure the fuel quantity during his preflight
inspection of the aircraft. No fuel was added. He
thought it odd that the pilot used the same,
moistened, end of the same stick to measure the
quantity in the second tank. The pilot commented
they wouldn't be out very long, maybe 1 hour.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's improper in-flight planning and decision
making, which resulted in exhaustion of the
airplane's fuel supply and loss of engine power.
= = =
Accident occurred Wednesday, December 19, 2001 in
San Diego, CA
Probable Cause Approval Date: 6/25/2003
Aircraft: Cessna T210N, registration: N7AL
Injuries: 3 Uninjured.
The airplane landed long and continued off the end
of the runway into a chain link fence. Nighttime
darkness prevailed and the airport weather, observed
3 minutes after the accident, was visibility 1/4
statute mile, vertical visibility 100 feet, with
temperature and dew point both 9 degrees Celsius. A
sheriff's deputy reported from the accident site
that the visibility was 50 to 100 yards in fog. The
pilot reported that the accident occurred as he was
returning to the departure airport following a
40-minute post maintenance checkflight. He received
the airport weather from the Automatic Terminal
Information Service (ATIS) recording and was aware
that ground fog had developed at the airport. He
received air traffic clearance and executed the
instrument landing system (ILS) approach. At
decision height he was still in visual
meteorological conditions and the runway and
approach lighting were in sight. The pilot continued
his descent below decision height
by visual reference and encountered dense fog and
severe restriction to visibility at 50 to 75 feet
above ground level. The pilot did not feel a
go-around was possible at that point and continued
the landing approach, landing long on the runway and
continuing off the end.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's failure to land on the runway with
sufficient runway remaining as a result of his
improper IFR procedure by his failure to maintain
visual contact with the runway environment, and to
execute a missed approach.
= = =
Accident occurred Thursday, February 15, 2001 in San
Diego, CA
Probable Cause Approval Date: 1/23/2002
Aircraft: Cessna 172N, registration: N4922D
Injuries: 2 Uninjured.
During landing rollout, the airplane veered off the
runway and collided with obstacles. At the
completion of a 3.7-hour-long flight, the tower
controller advised the pilot that the local wind was
from 270 degrees at 6 knots, and asked him to switch
runways to the parallel. After touchdown, the
airplane was still traveling about 50 knots when,
approaching runway 28L's midfield location, the
pilot lost directional control. The left wing rose
upward. The airplane veered off the runway and
impacted a sign. Airport personnel reported that the
collision occurred about 1,000 feet upwind of the
runway's threshold. The airplane came to a stop
about 550 feet farther upwind of the sign and about
200 feet north of the runway. No mechanical
malfunctions were reported with the airplane.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's failure to maintain directional control
of the airplane during landing rollout.
= = =
Accident occurred Thursday, February 08, 2001 in San
Diego, CA
Probable Cause Approval Date: 1/23/2002
Aircraft: Piper PA-28-181, registration: N8122G
Injuries: 1 Uninjured.
The pilot repositioned the engine fuel tank selector
to what he believed was the opposite wing tank when
in the downwind leg of the airport traffic pattern.
On the base leg, all engine power was lost and the
pilot performed an emergency landing, coming to rest
about 1,800 feet short of the runway's threshold. An
examination of the airplane revealed fuel in both
wing tanks. The pilot acknowledged that he had
mispositioned the fuel selector by inadvertently
switching it to the off position.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
Fuel starvation due to the pilot inadvertently
shutting off its supply on approach for landing.
Montgomery Field
Airport Approach / Landing: