This
is a publicly owned, class D airport with commercial service to Las Vegas.
Like many of California's airports, Stockton Metropolitan Airport has
declined in recent years. The terminal building has a cafe and lounge and
meeting space is available. In addition to the primary runway, Stockton
Airport has a 4,458 ft, 75 ft, general aviation runway. The future is
unclear, as new commercial and residential development encroaches on runway
buffer zones.
The
Stockton Metropolitan Airport is location on the south edge of Stockton
between Interstate 5 on the west and State Highway 99 on the East. Stockton
Airport
Originally called simply, Stockton Field,
and officially dedicated on January 11, 1941, a small municipal airport
became the oldest advanced flying school in the WFTC. Stockton Airport
Aerial Photo
Aero Turbine; Atlantic Aviation; Big Valley Aviation; Creative Aviation,
Inc.; Inland Flying Service; RJ Tuft Aviation; The Flight Center; Top Gun
Aviation; Vintage Aircraft; Wolfe Aviation; Public transportation;
limousines; Taxis; Rental cars available; Restaurant on the field; Top
Flight Cafe; Lodging within 4 miles;
Airport Stockton Airport Accident History:Accident occurred Saturday,
November 28, 2009 in Stockton, CA
Probable Cause Approval Date: 3/23/2010
Aircraft: PIPER PA-18-150, registration: N83516
Injuries: 1 Uninjured.
The pilot was landing at an airport. He requested to land on a taxiway next
to runway 29L. The air traffic control tower controller cleared the airplane
to land on the taxiway; however, the pilot landed the airplane in the grass
next to the taxiway. The pilot reported that during the landing roll, a gust
of wind lifted the right wing. He did not have enough control authority to
correct the elevated wing and the airplane nosed-over. The Federal Aviation
Administration inspector examined the airplane and noted that the rear spar
on the right wing was broken. At the time of the landing, the winds were
reported from 350 at 22 knots, gusting to 30 knots.
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Accident occurred Wednesday, October 31, 2007 in Stockton, CA
Probable Cause Approval Date: 12/20/2007
Aircraft: Piper PA-18-150, registration: N4153M
Injuries: 2 Uninjured.
The pilot reported that while taxing the tailwheel-equipped airplane into
position for takeoff from a private airstrip, the main landing gear struck a
ditch stopping the aircraft's forward movement almost instantly.
Subsequently, the aircraft nosed over and came to rest in an inverted
position. Examination of the aircraft by the pilot revealed that the rudder
and two lift struts were bent. The pilot reported no mechanical anomalies
with the aircraft at the time of the accident.
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On September 30, 2007, about 1515 Pacific daylight time, a Piper
PA-32R-301T, N4175A, landed with retracted landing gear at the Stockton
Metropolitan Airport, Stockton, California, following a hard landing at
another airport. The airplane was registered to N4175, LLC, and it was
operated by the company's owner on a personal flight. The airplane was
substantially damaged, and neither the private pilot nor passenger was
injured. Visual meteorological conditions prevailed at the time, and no
flight plan had been filed. The flight was performed under the provisions of
14 CFR Part 91, and it originated from San Carlos, California, about 1330.
In pertinent part, the pilot reported to the National Transportation Safety
Board investigator that his planned destination was the Pine Mountain Lake
(uncontrolled) Airport, Groveland, California. He had landed at Pine
Mountain during the past 4 to 6 years, and he was familiar with the runway
environment.
Pine Mountain's runway 09/27 is 3,625 feet long and 50 feet wide. The runway
has an asphalt surface.
The pilot reported that the flight to Pine Mountain was uneventful. During
his approach to runway 27 he noted that the wind was from the south, so he
placed the airplane into a crab on the final approach leg. The pilot
reported that nearing the runway and "just before coming over the threshold"
about 20 feet above the ground, "there was a sudden downdraft and the plane
rapidly and suddenly sunk toward the ground." The right main landing gear
impacted the gravel and dirt area about 10 feet in front and to the right of
the runway. The pilot aborted the landing and performed a go-around.
Ground-based witnesses observed the mishap and informed the pilot that the
airplane's landing gear appeared damaged. The pilot diverted to Stockton
where he made an intentional gear up landing.
The airplane was examined by Federal Aviation Administration personnel
following its removal from Stockton's runway. The right main landing gear
was found broken, structural components in the right wing were found
deformed, and the right side of the fuselage was buckled at the bulkhead aft
of the wing-to-fuselage attachment point.
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Accident occurred Thursday, April 12, 2007 in Stockton, CA
Probable Cause Approval Date: 6/27/2007
Aircraft: Cessna 172M, registration: N9685Q
Injuries: 1 Minor.
After a loss of engine power, the airplane landed short of the runway,
collapsing the nose gear and buckling the engine firewall. The pilot
departed with both fuel tanks full. His route of flight usually takes 3
hours to fly. He encountered turbulence and strong winds, which had the
effect of increasing the flight time to 4 hours. As he lined up for a
straight-in approach to the runway, the engine stopped due to fuel
exhaustion. The pilot executed a forced landing short of the approach end of
runway and collided with the ground and a fence. The pilot stated that the
airplane and engine had no mechanical malfunctions. An FAA inspector
examined the airplane at the accident scene and confirmed that there was no
fuel onboard.
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On April 1, 2007, at 1100 Pacific daylight time, a Cessna 320E, N3424Q,
collapsed the right main landing gear while exiting runway 29L at Stockton
Metropolitan Airport (SCK), Stockton, California. The pilot/owner operated
the airplane under the provisions of 14 CFR Part 91 as a personal flight.
The airplane sustained substantial damage. The pilot, the sole occupant, was
not injured. Visual meteorological conditions prevailed for the local area
flight that departed SCK about 1000. No flight plan had been filed.
According to the pilot, this was the first flight after an annual
inspection. He had flown to Calaveras County-Maury Rasmussen Field Airport
(CPU), San Andreas California, refueled, and then flew back to SCK. The
pilot noted no mechanical problems with the airplane during the flight until
he reached SCK. He stated that the landing and landing rollout were normal.
While slowing down to exit the high speed taxiway, he engaged the left
rudder to turn to the left, and the right main landing gear collapsed. The
right wing struck the runway, and right propeller and right horizontal
stabilizer were also damaged. The pilot reported that he exited onto the
taxiway at 20 miles per hour (mph). He further reported that during the
annual inspection the landing gear had been rerigged.
Reported winds at the time of the accident were variable at 3 knots.
TEST AND RESEARCH
According to a Federal Aviation Administration (FAA) inspector, the right
main landing gear bellcrank (part number 0841225-10) strut attachment bolt
(AN4-25A) sheared. This placed an increased load on the remaining main strut
attachment clevis ears, which caused the ears to fail and the down lock link
assembly to collapse. The FAA inspector stated that his inspection was not
able to ascertain whether or not the landing gear had been rigged
improperly.
The pilot had the landing gear independently inspected. According to the
inspection report, the right side main landing gear fork bolt was deformed
in an outward direction at the fork-to-bolt junction. The right main landing
gear down indicator switch had been rigged to a point where it made contact
at the "earliest possible moment during landing gear extension." The right
main landing gear fork bolt had been adjusted to what appeared to be its
full outboard limit. The right main landing gear outboard push pull tube rod
ends had been adjusted to their shortest possible length. The right landing
gear lock link end fitting and the right main landing gear bellcrank were
sent to a metallurgical laboratory that reported that the components had
failed in overload.
The aircraft logbook entry indicated that the annual inspection had been
completed and returned to service in an airworthy condition on April 1,
2007. The entry stated in part that the landing gear had been rigged in
accordance with Cessna's service manual.
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On January 24, 2007, about 1300 Pacific standard time, a Ross Hummer Pitts
Special, N41HR, nosed over following a loss of control during an aborted
takeoff on runway 29L at Stockton Metropolitan Airport, Stockton,
California. The commercial pilot, the sole occupant, received minor
injuries, and the airplane sustained substantial damage. The airplane was
registered to and operated by the pilot. Visual meteorological conditions
prevailed for the local personal flight conducted under 14 CFR Part 91, and
no flight plan was filed. The flight was originating when the accident
occurred.
During a telephone interview conducted by the NTSB investigator-in-charge on
January 25, 2007, the pilot reported that as he added power on the takeoff
roll, the engine rpm increased to 1,800 rpm and then stopped increasing. He
decided to abort the takeoff and reduced the power. By this time, the tail
wheel was off the ground, and he was using the rudder to steer the airplane.
The airplane began to turn to the right, so he applied left brake to stop
the turn, and the airplane "tipped upside down."
In a written statement, the pilot reported that during the takeoff roll, he
"thought there was a slight loss of power." He decided to abort the takeoff
and reduced the power. At a speed of about 30 mph, the airplane "suddenly
turned sharply as if one of the wheels went into a hole or rut." The pilot
applied opposite rudder and brake, but could not stop the turn. The airplane
nosed over and came to rest in the inverted position. The pilot stated that
the accident was due to "a hole or rut in the pavement or debris such as a
piece of aircraft tire."
An FAA inspector responded to the accident site. The inspector reported that
runway 29L had two grooved depressions running the length of the runway in
the asphalt on either side of the centerline. The grooves had a V shape and
were about 4 inches wide and 1 inch deep. The width of the grooves
corresponded to the width of the tires installed on the main landing gear of
the accident airplane.
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On May 30, 2005, about 1415 Pacific daylight time, a Cessna 172N, N172MR,
veered off runway 29R, and came to rest inverted at Stockton Metropolitan
Airport (SCK), Stockton, California. The pilot was operating the airplane
under the provisions of 14 CFR Part 91. The student pilot, the sole
occupant, was not injured; the airplane sustained substantial damage. The
cross-country personal flight departed Lincoln Regional Airport/Karl Harder
Field (LHM), Lincoln, California, about 1330, with a planned destination of
Stockton. Visual meteorological conditions prevailed, and no flight plan had
been filed.
The pilot submitted a written statement. He reported that on the landing
rollout, he applied the right brake too hard, and the airplane drifted to
the right and off the runway. The airplane hit a low spot in the dirt and
nosed over. The pilot stated that there were no mechanical discrepancies
noted with the airplane and engine.
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