Cable Airport, Upland, CA
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Airport Area Accident History:
Accident occurred Monday, June 04, 2007 in
Upland, CA
Probable Cause Approval Date: 9/26/2008
Aircraft: Piper PA-34-200, registration:
N4463T
Injuries: 1 Serious, 2 Minor.
A Certified Flight Instructor (CFI) was
providing multiengine instruction to the
pilot. They were in the traffic pattern,
approximately 800 feet above ground level (agl),
after completing several touch-and-go
landings. The CFI stated that his regular
method for setting up practice engine-out
landings for a student was to close the
mixture, allow the student to go through the
process of controlling the airplane, and
simulating the procedures to feather the
inoperative engine's propeller. The
instructor would then return the mixture to
full rich, and verify engine operation. This
would occur on downwind, and then the
landing would be completed with the
simulated inoperative engine at idle. On
downwind, the instructor closed the mixture
on the left engine. During this maneuver,
the pilot turned the airplane left from base
to final and the airspeed decreased. The
airplane rolled sharply to the left and lost
altitude. The instructor reduced both
throttles and
regained control of the airplane just as it
collided with the roof of one house, bounced
across another roof, and came to rest on top
of a third house. The Federal Aviation
Administration recommends that in-flight
simulated engine failures at altitudes below
3,000 feet agl be introduced only by
reduction of the throttle. Post-crash
inspection of the engine and airframe found
no anomalies that would have prevented
normal operation.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
Failure of the pilot under instruction to
maintain the minimum single engine control
airspeed (air) and directional control while
turning to final approach. Also causal was
the flight instructor's inadequate
supervision and delayed remedial actions.
= = =
Accident occurred Saturday, February 24,
2007 in Upland, CA
Probable Cause Approval Date: 9/27/2007
Aircraft: Scherer Europa, registration:
N81EU
Injuries: 2 Uninjured.
The pilot said that he was departing on
runway 24, and at approximately 80 feet
above the runway, the engine lost power. He
established a glide for a forced landing.
The aircraft impacted a berm on the left
side of the west end of the runway, bounced,
and came to rest about 150 feet from the
runway end. The engine compartment was
broken from the fuselage at the firewall,
and remained attached to the fuselage by
control cables and wires. The pilot said
that he had just finished a conditional
inspection. He said that he put 5 gallons of
fuel in the airplane prior to flight; it
holds a maximum of approximately 18 gallons.
He said that after the accident he found the
fuel line, which led to the fuel filter, to
be deteriorated. The pilot said that a small
piece of rubber from the fuel line was
blocking the filter's inlet. He believes
that this was what led to the fuel
starvation of the engine.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The pilot's inadequate condition inspection
and subsequent loss of engine power due to
fuel starvation as a result of a blocked
fuel filter.
= = =
Accident occurred Sunday, October 08, 2006
in Upland, CA
Probable Cause Approval Date: 3/31/2008
Aircraft: Robinson R22 Beta, registration:
N821SH
Injuries: 2 Uninjured.
The helicopter's engine suddenly lost power
during initial climb on an instructional
flight. The certified flight instructor
(CFI) took the controls and autorotated to a
hard touchdown in a gravel pit. After
securing the helicopter, the CFI inspected
the throttle linkage. He reported that
something appeared disconnected behind the
firewall. "When rotating the throttle from
full open to full close, the push/pull tube
that connects to the carburetor does not
move." The subsequent examination of the
helicopter's throttle spring assembly
revealed that on a previous occasion
improper maintenance had been performed. The
helicopter's maintenance records did not
reflect maintenance in this area. The
inspection revealed that the upper rod end
bearing was disconnected from the lower
portion of the rod because it had not been
safety wired as required. This maintenance
error resulted in a total loss of throttle
control.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
Disconnection of the throttle control
linkage due to improper maintenance, which
resulted in a loss of engine power during
initial climb.
= = =
Accident occurred Saturday, June 24, 2006 in
Upland, CA
Probable Cause Approval Date: 7/25/2007
Aircraft: Cessna 560, registration: N486SB
Injuries: 1 Fatal, 2 Serious.
The airplane touched down at night about
1,400 feet down the 3,864-foot runway and
overran the runway surface, coming to rest
about 851 feet beyond the departure end. The
pilot was operating the airplane using a
single-pilot waiver that he obtained two
months prior to the accident. The airplane
was certified by the Federal Aviation
Administration with a flight crew of two.
The pilot was returning from a personal
event with his family, and landing at his
home airport when the accident occurred.
Witnesses stated that the pilot’s approach
into the airport was not consistent with
previous approaches in which the airplane
would touch down directly on the runway
numbers. They also stated that they heard
the thrust reversers deploy, and then return
to the stowed position. The airplane flight
manual states that once the thrust reversers
have been deployed, a pilot should not
attempt to restow the thrust reversers and
take off. Two sink rate warnings were
issued during the approach to landing which
should have alerted the pilot of the
unstabilized approach. Performance
calculations showed that the airplane would
have required an additional 765 to 2,217
feet of runway for a full stop landing.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The pilot's unstabilized approach to the
runway and failure to obtain the proper
touchdown point, which resulted in a runway
overrun.
= = =
Accident occurred Wednesday, October 19,
2005 in Upland, CA
Probable Cause Approval Date: 2/28/2006
Aircraft: Piper PA-23-160, registration:
N4252P
Injuries: 1 Minor, 2 Uninjured.
After touchdown, the airplane veered off the
right side of the runway and collided with a
vehicle. During the collision sequence, the
airplane spun 180 degrees and its right main
landing gear collapsed. The pilot said that
following the airplane's touchdown on the
runway, he started to apply the brakes but
they felt mushy and unresponsive. He applied
more and more pressure to the brakes but the
airplane did not stop. As he continued to
apply pressure, the airplane departed the
right side of the runway and collided with a
vehicle. A Federal Aviation Administration
(FAA) airworthiness inspector examined the
braking system with an aviation maintenance
technician. The left brake had new linings
and the brake disk was worn. The right brake
linings were at a minimum and the disk was
within acceptable limits. Responding law
enforcement officers noted that three
distinctive skid marks matching the
dimensional geometry of the aircraft's
landing gear were on the
runway and they veered for several hundred
feet off the right side of the runway and
led to the impact damaged vehicle and the
airplane. The skid marks corresponding to
the right and left main wheels were
identical in width, heaviness, and color.
The FAA inspector reported that there was no
evidence that either brakes had locked up
during the landing.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
the pilot's failure to maintain directional
control during landing.
= = =
Accident occurred Friday, August 20, 2004 in
Upland, CA
Probable Cause Approval Date: 10/28/2004
Aircraft: Berry Hatz CB-1, registration:
N592DJ
Injuries: 1 Uninjured.
The airplane veered off the runway and
collided with a taxiway light, followed by a
collision with a hangar. The airplane
bounced upon initial touchdown onto the
runway. The pilot added power to soften the
following touchdown and the airplane veered
to the left and collided with a taxiway
light and then a hangar. The pilot said that
the bi-wing structure of the airplane
reduced his forward visibility and made
regaining runway alignment difficult. The
pilot noted no mechanical problems with the
airplane prior to the accident.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
the pilot's inadequate recovery following a
bounced landing, improper use of the rudder
control, and failure to maintain directional
control.
= = =
Accident occurred Friday, February 13, 2004
in Upland, CA
Probable Cause Approval Date: 4/28/2005
Aircraft: Cessna 172N, registration: N5107K
Injuries: 2 Minor, 1 Uninjured.
The engine lost partial power just after the
airplane lifted off the runway and the pilot
aborted the takeoff and attempted to land on
the remaining runway. The airplane touched
down on the runway, overran its departure
end, impacted a flatbed trailer, and came to
rest on uneven terrain against a berm about
43 yards from the runway. The pilot reported
that the airplane appeared to have been in
proper working condition and worthy of
flight during his preflight and pretakeoff
inspections. However, after climbing for
several seconds he heard the engine lose
power, and its tachometer decreased to 1,400
rpm. The pilot believed that the airplane
was not going to continue flying so he
elected to abort the takeoff. To ascertain
the reason for the power loss, the accident
airplane's engine was removed from the
airplane and installed on another airframe.
After removing and replacing several
impact-damaged engine
accessories/components, the engine was run
up to
2,400 rpm. With the exception of a minor
vibration due to the fact that the
crankshaft was bent, the engine operated
normally. The reason for the partial engine
power loss, as reported by the pilot, was
not ascertained.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
A partial loss of engine power for
undetermined reasons during takeoff.
= = =
Accident occurred Saturday, June 03, 2000 in
UPLAND, CA
Probable Cause Approval Date: 7/30/2001
Aircraft: Mooney M20F, registration: N9207V
Injuries: 1 Minor, 3 Uninjured.
The airplane veered off the runway and came
to rest in a ditch during takeoff. The pilot
reported that the cabin door came open
during takeoff. He intended to continue the
takeoff and return to land and close the
door; however, the passenger in the right
front seat distracted him. In the time
necessary to calm and reassure the
passenger, the pilot lost directional
control of the aircraft and it drifted off
the runway to the left. The nearest aviation
surface weather observation, at an airport 6
miles away, was reporting calm wind
conditions.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The failure of the pilot-in-command to
maintain directional control of the aircraft
on takeoff after the cabin door became ajar.
= = =
Accident occurred Saturday, January 08, 2000
in UPLAND, CA
Probable Cause Approval Date: 1/2/2002
Aircraft: Clark PITTS S1X, registration:
N900SH
Injuries: 1 Fatal.
During an air show, while conducting
aerobatic maneuvers, the airplane continued
in a spin to ground impact. According to
witnesses, the pilot was performing an
aerobatic routine with two other airplanes,
known as a "squirrel cage" maneuver. The
airplanes would take turns entering the
aerobatic box to perform a single
choreographed maneuver. The routine card
indicated that the pilot was to perform
multiple snap rolls when the accident
occurred. A video of the pilot's routine was
examined with the assistance of members of
the International Aerobatic Club. The video
showed that the pilot made 3 1/2 snap rolls
to the right, and then 2 1/2 spins to the
left. It appeared there was no flight
control problem and the pilot entered a flat
spin. The elevator appeared to be loaded and
the pilot never broke the stall prior to
impact. The pilot had written a magazine
article advocating a specific spin recovery
method.
The National Transportation Safety Board
determines the probable cause(s) of this
accident as follows:
The pilot's failure to recover from an
intentional aerobatic maneuver.
Cable
Airport Approach / Landing: