Glenn County Airport, Willows, CA
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Airport Area Accident History:
Accident occurred Friday, April
28, 2006 in
Willows, CA
Probable Cause Approval Date:
10/31/2006
Aircraft: Cirrus SR-20,
registration: N1488C
Injuries: 1 Uninjured.
The airplane incurred structural
damage during landing when the
airplane entered a porpoise
pilot induced oscillation and
the propeller struck the runway.
The student pilot was on the
second leg of his solo
cross-country flight. The
approach to runway 34 was
normal, but during touchdown the
airplane porpoised. The pilot
initiated an aborted landing,
and flew the airplane to
Red Bluff Municipal Airport
where he landed uneventfully. He
parked the airplane at the ramp
and shut down the engine. The
pilot inspected the airplane and
found damage to the propeller
resulting from ground impact
during the porpoise. An
inspection by maintenance
personnel revealed structural
damage. The pilot stated that
the airplane and engine had no
mechanical failures or
malfunctions during the flight.
The National Transportation
Safety Board determines
the probable cause(s) of this
accident as follows:
the pilot's misjudged landing
flare and improper recovery from
a bounced landing.
===
Accident occurred Sunday, May
08, 2005 in Willows, CA
Probable Cause Approval Date:
5/30/2006
Aircraft: Grumman G-164C,
registration: N6535K
Injuries: 1 Uninjured.
The pilot force landed the
airplane in a rice field
following a loss of engine power
and the main landing gear was
sheared off after contacting a
berm. While the pilot was
seeding rice over a field, the
engine lost partial power. The
pilot force landed the airplane
in a field. During the landing
roll, the landing gear impacted
a berm and were sheared from
their structural attachment
points on the airplane. Until
the ground impact, the engine
was producing partial power, but
not enough to sustain flight.
Post accident inspection of the
engine by the
Federal Aviation Administration
accident coordinator revealed
that the number 5 cylinder
piston had fractured at the
piston pin boss. The piston pin,
which is mounted in the piston
pin boss and holds the piston to
the
connecting rod, fell from
the boss and the connecting rod
was free to rotate. The engine
was overhauled about 1,154 hours
prior to the accident. The
maintenance history on the
piston could not be determined
based on available records.
The National Transportation
Safety Board determines the
probable cause(s) of this
accident as follows:
the loss of engine power due to
the fractured piston pin boss on
the number 5 cylinder.
===
Accident occurred Wednesday, May
21, 2003 in Willows, CA
Probable Cause Approval Date:
12/28/2004
Aircraft: Ayres S2R-T34,
registration: N5653X
Injuries: 1 Uninjured.
The
commercial pilot was
making a steep turn during an
agricultural
aerial applicationwhen
the airplane's engine lost
power. He made a forced landing
in a field, and in the process,
the airframe received structural
damage. The pilot said he had
ground crew fuel the left tank
of the airplane with the engine
still running. He completed
three loads, with each load
cycle taking about 12 minutes.
He then performed a steep turn
of about 70-degrees to complete
one last pass. About 400 above
ground level, the engine lost
power and he was unable to
restart it. He landed the
airplane in the field below, and
the airplane skidded about 100
feet and nosed over. The person
who recovered the airplane did
not observe any fuel in the
airplane fuel tanks, or
at the accident site.
The National Transportation
Safety Board determines the
probable cause(s) of this
accident as follows:
A loss of engine power for an
undetermined reason during an
aerial application.
===
Accident occurred Wednesday,
August 21, 2002 in Willows, CA
Probable Cause Approval Date:
9/29/2004
Aircraft:
Cessna 195, registration:
N4344V
Injuries: 2 Uninjured.
The pilot failed to maintain
runway alignment during the
landing flare, which resulted in
the airplane touching down off
the runway in soft dirt and
nosing over. The pilot had just
purchased the tail wheel
equipped airplane and was
practicing touch-and-go takeoffs
and landings to gain confidence
in the airplane prior to flying
it home. The pilot said that
during the first landing, about
2 feet above the ground, the
airplane was "blown" to the
right of the runway where it
touched down in the soft dirt.
The main tires dug into the
dirt, and the airplane nosed
over. The pilot reported that
having more flight time in the
airplane may have helped prevent
the accident. He had 5 hours in
this make and model of airplane.
The National Transportation
Safety Board determines the
probable cause(s) of this
accident as follows:
the pilot's inadequate
compensation for crosswind
conditions resulting in his
failure to maintain runway
alignment. Contributing factors
to the accident were the pilot's
lack of familiarity with the
airplane.
===
Accident occurred Thursday,
April 11, 2002 in Willows, CA
Probable Cause Approval Date:
6/30/2004
Aircraft: Beech G35,
registration: N4487D
Injuries: 2 Fatal.
According to witnesses, the
airplane was seen approaching
the motor sports park from the
southwest at approximately 1,200
feet agl and at a "faster than
usual" rate of speed. The
airplane was in a "sharp,
90-degree bank," as it began to
circle the park in a level turn.
After circling around to the
east, the airplane returned to a
wings-level attitude and began
to climb. Shortly thereafter,
the tail of the airplane began
to "shake violently" and
separate from the airplane. One
witness said he heard a loud
noise as "the tail came off, and
all of it started falling
apart." He said the tail section
separated first, then the
airplane pitched over, and the
left wing broke off. Witnesses
saw the airplane enter a
downward spiral. As the airplane
descended, the engine separated
and the passenger was ejected.
The airplane then entered an
inverted flat spin and impacted
the ground 1,000 feet north of
park. An examination of the
airplane's left wing, and
stabilizers revealed structural
failures consistent with
overload. According to the
manufacturer's Flight Strength
Diagram or Vn diagram for the
G35, abrupt control column
deflection at a speed of 113
knots (Va, or
maneuvering speed) could
produce a 4.4 G structural load
(Limit Load factor), while
abrupt control column deflection
at or above 152 knots (Vno/Vc,
or maximum structural cruise
speed) could produce a 6.6 G
structural load (Ultimate
Load limit ). Examination
of the recorded radar data
disclosed that the airplane was
traveling at 142 knots at the
time of the breakup.
Engineering analysis
concluded that in a level turn,
the bank angle required to
achieve
Limit Load is 76.8
degrees, and the bank angle
required to achieve the Ultimate
Load is 81.2 degrees. FAA
toxicology testing of the pilot
revealed the presence of
Diphenhydramine in urine, and
Norverapamil, and Verapamil in
urine and liver.
The National Transportation
Safety Board determines the
probable cause(s) of this
accident as follows:
the pilot's entry into an abrupt
maneuver at an excessive
airspeed beyond Va, which
resulted in exceeding the
aircraft's design stress limits.
===
Accident occurred Friday, June
16, 2000 in WILLOWS, CA
Probable Cause Approval Date:
10/17/2001
Aircraft: Maule M4-210C,
registration: N377BC
Injuries: 2 Fatal.
A witness saw the airplane
complete the second and last set
of two 360-degree turns just
above treetop level over a herd
of antelope and then descend to
ground impact in a steep nose
down attitude. This airplane was
the last in a group of six other
aircraft going to the same
destination. Initial responders
to the accident site said that a
herd of antelope was in the
immediate vicinity of the
wreckage. Interviews with the
other pilot's in the group
revealed that both the pilot and
passenger were avid animal
lovers. They heard the pilot
announce in a normal voice that
he was turning downwind to base
on the
Common Traffic Advisory
Frequency (CTAF). No
other transmissions were heard
from the airplane. The ground
witness saw the airplane flying
northbound at low level, and
then enter the first set of
steep 360-degree turns. The
airplane ended this maneuver
descending towards the ground in
wings level flight and then
rising up again, with a turn
southbound. The airplane climbed
above the tree line, leveled
off, and then entered the second
set of steep 360-degree turns,
which culminated in the
accident. Winds in the area were
recorded from the
north-northwest at 32 mph
gusting to 42 mph. As the pilot
turned from crosswind to
downwind while in a steep turn
about the antelope herd on the
ground, it is likely that the
airplane encountered
strong wind shear like
tailwind condition, which
resulted in an inadvertent
stall/spin. There were no
discrepancies noted with the
aircraft and engine.
The National Transportation
Safety Board determines the
probable cause(s) of this
accident as follows:
Failure of the pilot to maintain
an adequate airspeed margin
while maneuvering in steep turns
at low altitude in gusty and
strong tailwind conditions,
which lead to a
wind shear encounter and
a stall/spin. A contributing
factor in the accident was the
pilot's diverted attention due
to looking at antelope on the
ground, and, his decision to
attempt the steep turns at low
altitude.
===
Accident occurred Saturday,
April 15, 2000 in WILLOWS, CA
Probable Cause Approval Date:
6/25/2003
Aircraft: Smith RV-4,
registration: N63SM
Injuries: 2 Minor.
The pilot reported that he lost
elevator control while in cruise
flight. He was attempting to
land at an airport on a runway
he was nearly aligned with.
Using the manipulation of
aircraft trim and throttle as a
means of controlling the
aircraft's pitch attitude, he
tried to gain altitude by
trimming the airplane in the
full aft position, but found the
elevator to be jammed. The pilot
reduced the throttle and mixture
and landed in a field. The
airplane came to rest in an
upright position. An FAA
inspector examined the airplane
following recovery and reported
that
control rod was
improperly installed, allowing
the rear jam nut on the elevator
push rod to work loose. The push
rod then rotated off the forward
connection.
The National Transportation
Safety Board determines the
probable cause(s) of this
accident as follows:
Disconnection of the elevator
push rod due to the
owner/builder's improper
installation of the rear jam nut
on the elevator pushrod.
Glenn County
Airport Approach / Landing: